Transmittal of NUREG-1190 Regarding the San Onofre Unit 1 Loss of Power and Water Hammer Event (Generic Letter No. 86-07)
UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 March 20, 1986 TO ALL REACTOR LICENSEES AND APPLICANTS Gentlemen: SUBJECT: TRANSMITTAL OF NUREG-1190 REGARDING THE SAN ONOFRE UNIT 1 LOSS OF POWER AND WATER HAMMER EVENT (GENERIC LETTER 86-07) On November 21, 1985, while operating at 60% power, Southern California Edison Company's San Onofre Unit 1 Nuclear Power Plant experienced a loss of ac electrical power followed by a severe water hammer in the secondary system which caused a steam leak and damaged plant equipment. Shortly after the event, the NRC Executive Director for Operations directed that an NRC Team be sent to San Onofre, in conformance with the recently established Incident Investigation Program, to investigate the circumstances of this event. The NRC Team has now completed its investigation and has documented the factual information and their findings and conclusions associated with the event (see enclosed NUREG-1190, entitled "Loss of Power and Water Hammer Event at San Onofre Unit 1, on, November 21, 1985"). In this report, the team has concluded that the event was significant because (a) all inplant ac power was lost for 4 minutes; (b) all steam generator feedwater was lost for 3 minutes; (c) a severe water hammer caused by check valve failures was experienced in the feedwater system which caused a leak, damaged plant equipment and challenged the integrity of the auxiliary feedwater system; (d) all indicated steam generator water levels dropped below scale; and (e) the reactor coolant system experienced an acceptable but unnecessary cooldown transient. In the team's view the most significant aspect of the event was that five safety-related feedwater system check valves degraded to the point of inoperability during a period of less than a year, without detection, and that their failure jeopardized the integrity of safety-related feedwater piping. The cause of the feedwater system check valve failures has been preliminarily identified by SCE as partial or complete separation of the check valve disc assemblies due to fluid flow conditions. Information submitted to the staff on this subject is currently under review. You should review the information in the enclosed report for applicability to your facility. In addition, you should ensure that the information in NUREG-1190 is made available to your plant staff as part of your training program in connection with the Feedback of Operating Experience to Plant Staff (TMI Action Plan Item I.C.5). 8603210334 March 20, 1986 - 2 - On February 4, 1986, the Executive Director for Operations (EDO) identified and assigned responsibility or generic and plant-specific actions resulting from the investigation of the San Onofre event. Some of the generic actions may be applicable to your facility. A copy of the EDO memorandum is included for your information. This generic letter is provided for information only, and does not involve any reporting requirements. Therefore, no clearance from the Office of Management and Budget is required. The enclosed report is currently under NRC review. Any generic requirements stemming from the report will be transmitted at a later date following completion of the appropriate procedural steps. Sincerely, Harold R. Denton, Director Office of Nuclear Reactor Regulation Enclosures: 1. NUREG-1190 2. EDO Memorandum of February 4, 1986 3. List of Generic Letters
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021