Event Notification Report for November 10, 2024
U.S. Nuclear Regulatory Commission
Operations Center
EVENT REPORTS FOR
11/09/2024 - 11/10/2024
EVENT NUMBERS
57418
57418
Power Reactor
Event Number: 57418
Facility: Grand Gulf
Region: 4 State: MS
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Melissa Limbeck
HQ OPS Officer: Ernest West
Region: 4 State: MS
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Melissa Limbeck
HQ OPS Officer: Ernest West
Notification Date: 11/10/2024
Notification Time: 07:59 [ET]
Event Date: 11/10/2024
Event Time: 03:37 [CST]
Last Update Date: 11/10/2024
Notification Time: 07:59 [ET]
Event Date: 11/10/2024
Event Time: 03:37 [CST]
Last Update Date: 11/10/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Dixon, John (R4DO)
Dixon, John (R4DO)
| Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
|---|---|---|---|---|---|---|
| 1 | M/R | Y | 100 | Power Operation | 0 | Hot Shutdown |
MANUAL REACTOR SCRAM
The following information was provided by the licensee via phone and email:
"On November 10, 2024, at 0337 CST, Grand Gulf Nuclear Station (GGNS) was operating in mode 1 at 100 percent power when a manual scram was initiated due to degrading main condenser vacuum. The cause of the degrading main condenser vacuum is not known at this time and is being investigated. All control rods fully inserted and there were no complications. Reactor pressure was initially maintained with main turbine bypass valves. Reactor water level was initially maintained with main feedwater and condensate.
"At 0457, operators transitioned pressure control to safety relief valves and began using reactor core isolation cooling (RCIC) to maintain reactor water level. This was performed using plant procedures due to degrading vacuum. GGNS is currently in mode 3. Reactor level is being maintained with RCIC and pressure is being maintained using the safety relief valves.
"The manual reactor protection system (RPS) actuation is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) and the RCIC actuation is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A).
"The NRC Senior Resident Inspector was notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
At the time of the notification, main steam isolation valves had shut on low vacuum.
* * * UPDATE ON 11/10/24 AT 1236 CST FROM MELISSA LIMBECK TO KERBY SCALES * * *
The following update was provided by the licensee via phone and email:
"This update is being made to report the following occurrences which took place after the scram reported in event number 57418.
"On November 10, 2024, at 0545 CST, a group 1 containment isolation signal resulted in the closure of all MSIVs. The signal was due to continued degradation of condenser vacuum post-trip. At 0620, an automatic RPS actuation occurred when reactor water level lowered to level 3. This RPS actuation occurred with all control rods fully inserted. Reactor water level lowered following closure of an open safety relief valve and was recovered to within the established band.
"The events are being reported as specified system actuations in accordance with 10 CFR 50.72(b)(3)(iv)(A).
"The NRC Senior Resident Inspector has been informed of the update."
Notified R4DO (Dixon)
The following information was provided by the licensee via phone and email:
"On November 10, 2024, at 0337 CST, Grand Gulf Nuclear Station (GGNS) was operating in mode 1 at 100 percent power when a manual scram was initiated due to degrading main condenser vacuum. The cause of the degrading main condenser vacuum is not known at this time and is being investigated. All control rods fully inserted and there were no complications. Reactor pressure was initially maintained with main turbine bypass valves. Reactor water level was initially maintained with main feedwater and condensate.
"At 0457, operators transitioned pressure control to safety relief valves and began using reactor core isolation cooling (RCIC) to maintain reactor water level. This was performed using plant procedures due to degrading vacuum. GGNS is currently in mode 3. Reactor level is being maintained with RCIC and pressure is being maintained using the safety relief valves.
"The manual reactor protection system (RPS) actuation is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) and the RCIC actuation is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A).
"The NRC Senior Resident Inspector was notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
At the time of the notification, main steam isolation valves had shut on low vacuum.
* * * UPDATE ON 11/10/24 AT 1236 CST FROM MELISSA LIMBECK TO KERBY SCALES * * *
The following update was provided by the licensee via phone and email:
"This update is being made to report the following occurrences which took place after the scram reported in event number 57418.
"On November 10, 2024, at 0545 CST, a group 1 containment isolation signal resulted in the closure of all MSIVs. The signal was due to continued degradation of condenser vacuum post-trip. At 0620, an automatic RPS actuation occurred when reactor water level lowered to level 3. This RPS actuation occurred with all control rods fully inserted. Reactor water level lowered following closure of an open safety relief valve and was recovered to within the established band.
"The events are being reported as specified system actuations in accordance with 10 CFR 50.72(b)(3)(iv)(A).
"The NRC Senior Resident Inspector has been informed of the update."
Notified R4DO (Dixon)