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Event Notification Report for March 17, 2024

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
03/16/2024 - 03/17/2024

EVENT NUMBERS
57033
Power Reactor
Event Number: 57033
Facility: Comanche Peak
Region: 4     State: TX
Unit: [2] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Kris Brigman
HQ OPS Officer: Sam Colvard
Notification Date: 03/17/2024
Notification Time: 17:59 [ET]
Event Date: 03/17/2024
Event Time: 15:15 [CDT]
Last Update Date: 03/17/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Werner, Greg (R4DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 M/R Y 100 Power Operation 0 Hot Standby
Event Text
MANUAL REACTOR TRIP DUE TO MAIN FEEDWATER PUMP TRIP

The following information was provided by the licensee via phone and email:

"On March 17, 2024, at 1515 CDT, the Comanche Peak Unit 2 reactor was manually tripped due to an anticipated automatic trip due to lo-lo steam generator (SG) water levels. Prior to the trip, main feedwater pump '2B' tripped and an auto runback to 700 MW (60 percent power) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs.

"Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedures IPO-007B. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves."

The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:

The cause of the '2B' main feed pump trip was due to loss of primary and redundant power to the servo control valve. The loss of power to the servo control valve is under investigation.