Event Notification Report for August 7, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/06/2003 - 08/07/2003 ** EVENT NUMBERS ** 39631 39941 40033 40049 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39631 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 03/02/2003| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 16:00[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 03/02/2003| +------------------------------------------------+EVENT TIME: 14:30[EST]| | NRC NOTIFIED BY: CHARLES PIKE |LAST UPDATE DATE: 08/06/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WALTER RODGERS R2 | |10 CFR SECTION: |DAVID AYRES R2 | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION TO STATE AGENCY OF EXPIRED GREEN SEA TURTLE FOUND AT | | BARRIER NET | | | | "NRC notification [is] being made due to state notification to [the] Florida | | Wildlife Commission regarding a Green Sea Turtle found dead at barrier net | | pursuant to 10 CFR 50.72(b)(2)(xi)." | | | | The turtle was found on the surface at the barrier net with no injuries or | | abnormalities except for fresh cuts common for turtles coming through pipes. | | The cause of death is unknown at this time. A necropsy is planned. | | | | The NRC Resident Inspector will be notified by the licensee. | | | | * * * UPDATE ON 3/15/03 @ 1033 EST FROM TEREZAKIS TO CROUCH * * * | | | | "On 3-15-03, a green sea turtle was retrieved from the plant's intake canal. | | The turtle was determined to be in need of rehabilitation. The injuries to | | the turtle are not causal to plant operation. Per the plant's turtle permit, | | the Florida Fish and Wildlife Conservation Commission (FWCC) was notified at | | 0920 EST. This non-emergency notification is being made pursuant to 10 CFR | | 50.72(b)(2)(xi) due to the notification of FWCC." | | | | The NRC Resident Inspector will be notified by the licensee. | | | | * * * UPDATE ON 3/19/03 AT 1222 EST FROM E. SUMNER TO RIPLEY * * * | | | | "On 03/19/03 @ 1105 hrs., one loggerhead turtle was retrieved from the | | plant's intake canal. The turtle was determined to be in need of | | rehabilitation. The injury to the turtle is not causal to plant operation. | | Per the plant's turtle permit, the Florida Fish and Wildlife Conservation | | Commission (FWCC) was notified at 1115 EST." | | | | The NRC Resident Inspector was notified. | | | | * * * UPDATED ON 3/31/03 AT 1159 EST FROM W.L. PARK TO A. COSTA * * * | | | | "On 3-31-03 [1105 EST], a loggerhead sea turtle was retrieved from the | | plant's intake canal. The turtle was determined to be in need of | | rehabilitation. The injuries to the turtle are not causal to plant | | operation. Per the plant's turtle permit, the Florida Fish and Wildlife | | Conservation Commission (FWCC) was notified at 1105 EST. This non-emergency | | notification is being made pursuant to 10 CFR 50.72(b)(2)(xi) due to the | | notification of FWCC." | | | | The NRC Resident Inspector will be notified. | | | | * * * UPDATE 1235EST ON 4/9/03 FROM ANDY TEREZAKIS TO S.SANDIN * * * | | | | "On 4-9-03, a loggerhead sea turtle was retrieved from the plant's Intake | | canal. The turtle was determined to be in need of rehabilitation. The | | injuries to the turtle are not causal to plant operation. Per the plant's | | turtle permit, the Florida Fish and Wildlife Conservation Commission (FWCC) | | was notified at 1100 EST. This non-emergency notification is being made | | pursuant to 10CFR50.72(b)(2)(xi) due to the notification of FWCC." | | | | The licensee informed the NRC resident inspector. Notified R2DO(Landis). | | | | *** UPDATE ON 5/2/03 AT 1826 FROM S. OEHRLE TO A. COSTA *** | | | | "On 5/2/03, a green sea turtle was retrieved from the intake canal. The | | turtle required rehabilitation. The injuries were not causal to plant | | operation. Per the plant's turtle permit, the Florida Fish and Wildlife | | Conservation Commission was notified at 1445 EDT. This non-emergency | | notification is being made pursuant to 10 CFR 50.72 (b)(2)(xi) due to | | offsite notification." | | | | The Licensee will notify the NRC Resident Inspector. Notified R2DO | | (Munday). | | | | **** update on 05/24/03 at 1417 EDT FROM JOE HESSLING TO JOHN MACKINNON | | **** | | | | "On 5-24-03, a loggerhead sea turtle was retrieved from the plant's intake | | canal. The turtle was determined to be in need of rehabilitation. The | | turtle was very underweight and lethargic, no injuries or anomalies noted. | | Turtle's condition is not causal to plant operation. Per the plant's turtle | | permit the Florida Fish and Wildlife Conservation Commission (FWCC) was | | notified at 1345 EDT. This non-emergency notification is being made | | pursuant to 10 CFR 50.72(b)(2)(xi) due to the notification of FWCC. NRC R2DO | | (TOM DECKER) notified. | | | | The NRC Resident Inspector was by notified of this event by the licensee. | | | | ****UPDATE ON 5/27/03 AT 10:49 FROM HESSLING TO LAURA**** | | | | "On 5-27-03, a loggerhead sea turtle was retrieved from the plant's intake | | canal. The turtle was determined to be in need of rehabilitation. The turtle | | was underweight, and missing lower posterior marginals on left side. | | Turtle's injuries are not causal to plant operation. Per the plant's turtle | | permit, the Florida Fish and Wildlife Conservation Commission (FWCC) was | | notified at 0850 EDT. This non-emergency notification is being made pursuant | | to 10 CFR 50.72(b)(2)(xi) due to the notification of FWCC." | | | | Notified R2DO (T. Decker) | | | | * * * UPDATE ON 06/17/03 AT 12:45 EDT FROM CALVIN WARD TO ARLON COSTA * * * | | | | "At approximately 12:45 p.m. on 6/17/03 a loggerhead turtle was rescued from | | the St. Lucie Plant intake canal. The turtle was injured and will be | | transported to the State authorized sea turtle rehabilitation facility. The | | Florida Dept. of Environmental Protection (FDEP) was notified at 1:09 p.m. | | as required by the St. Lucie Plant Sea Turtle Permit - see the attached sea | | turtle stranding report (1 page). | | | | "Notification to the state government agency requires a four (4) Hr. | | Non-Emergency Notification to the NRC per 10 CFR 50.72(b)(2)(xi). There were | | no unusual plant evolutions in progress which may have contributed to this | | event." | | | | The licensee notified the NRC Resident Inspector. | | | | Notified R2DO (L. Wert). | | | | * * * UPDATE 0605 EDT ON 6/26/03 FROM STEVE MERRILL TO S. SANDIN * * * | | | | The licensee was informed by the FWCC that the green sea turtle requiring | | rehabilitation which was retrieved from the plant's intake canal on 3/15/03 | | had expired within 10 days of removal. Consequently, the licensee is | | updating their 3/15/03 report to include this additional information. The | | licensee will inform the NRC Resident Inspector. Notified R2DO(C. Ogle). | | | | * * * UPDATE 1506 EDT ON 07/01/03 FROM CALVIN WARD TO GOTT * * * | | | | On 04/02/03, a green sea turtle was retrieved from the intake canal. The | | turtle required rehabilitation. The injuries were not causal to plant | | operation. Per the plant's turtle permit, the Florida Fish and Wildlife | | Conservation Commission was notified. This non-emergency notification is | | being made pursuant to 10 CFR 50.72 (b)(2)(xi) due to offsite notification. | | On 07/01/03 licensee QA discovered that the injury had occurred and that the | | NRC had not been notified within the 4 hours. The failure to report the | | event within the regulatory time is being investigated and has been entered | | into the stations corrective action program. | | | | The licensee notified the NRC Resident Inspector. | | | | Notified R2DO (Munday) | | | | * * * UPDATE 1750 EDT ON 07/07/03 FROM JOE HESSLING TO MACKINNON * * * | | | | On 07/07/03, a Loggerhead sea turtle was retrieved from the plants' intake | | canal. The turtle was determined to be in need of rehabilitation. The | | injuries to the turtle are not causal to plant operation. Per the plant's | | Turtle permit, the Florida Fish and Wildlife Conversation Commission (FWCC) | | was notified at 1715 EDT. This non-emergency is being made pursuant to 10 | | CFR 50.72(b)(2)(xi) due to the notification of FWCC. | | | | The licensee notified the NRC Resident Inspector. | | | | Notified R2DO (Munday). | | | | | | * * * UPDATE ON 07/25/03 @ 1510 BY CALVIN WORD TO STEVE SANDIN * * * | | | | On 7/25/03, a sea turtle was retrieved from the plant's intake canal. The | | turtle was determined to be in need of rehabilitation. The injuries to the | | turtle are not causal to plant operation. Per the plant's turtle permit, | | the Florida Fish and Wildlife Conservation Commission (FWCC) was notified. | | This non-emergency notification is being made pursuant to 10 CFR | | 50.72(b)(2)(xi) due to the notification of FWCC. | | | | The licensee notified the NRC Resident Inspector and other Government | | Agencies | | | | Reg 2 RDO(Anne Boland) was informed | | | | * * * UPDATE ON 08/06/03 AT 1611 BY ALAN HALL TO ARLON COSTA * * * | | | | "On 08/06/03 [at 1410], a sea turtle was retrieved from the plant's intake | | canal. The turtle was determined to be in need of rehabilitation. The | | injuries to the turtle are not causal to plant operation. Per the plant's | | turtle permit, the Florida Fish and Wildlife Conservation Commission (FWCC) | | was notified. This non-emergency notification is being made pursuant to 10 | | CFR 50.72(b)(2)(xi) due to the notification of FWCC. Stranding Report copy | | attached." | | | | The licensee will notify the NRC Resident Inspector. | | | | Notified R2DO (Stephen Cahill). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 39941 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GUTHRIE HEALTH CARE |NOTIFICATION DATE: 06/16/2003| |LICENSEE: GUTHRIE HEALTH CARE |NOTIFICATION TIME: 09:20[EDT]| | CITY: SAYRE REGION: 1 |EVENT DATE: 06/12/2003| | COUNTY: STATE: PA |EVENT TIME: [EDT]| |LICENSE#: 37-01893-01 AGREEMENT: N |LAST UPDATE DATE: 08/06/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |RAYMOND LORSON R1 | | |DOUG BROADDUS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOON PARK | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LDIF 35.3045(a)(1) DOSE > PRESCRIBED DOSA| | |LOTH 35.3045(a)(3) DOSE TO OTHER SITE > SP| | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT PART OF THE IMPLANTED SEEDS WERE NOT IN THE PROPER SITE | | | | A patient was referred for treatment, due to reoccurring prostate cancer, to | | the hospital where he had previously had treatment. Seeds were implanted | | around May 2001. A scan of the previous treatment of implanted seeds | | determined that many of the seeds were not located in the prostate, but in | | adjacent tissue where they would have been ineffective in treatment. Also, | | a review of the records indicated a scan was performed in early 2002, but | | was not followed up on. The patient and referring physician have been | | informed. The hospital is conducting an investigation into the event and | | also developing a plan to provide appropriate treatment for the patient. | | | | * * * UPDATE ON 07/18/03 AT 1638 FROM JOON PARK TO ARLON COSTA * * * | | | | Post-op dosimetry on one patient was determined to be a misadministration. | | The dose that covered the prostate was more than 20 percent different from | | the prescription as well as the penile bulb dose being close to 50 percent | | of the prescription dose. Efforts are being made to contact the affected | | patient. The licensee will continue efforts to obtain post-op dosimetry on | | the rest of the patients related to this incident so that evaluations for | | misadministration can be performed. | | | | Notified R1DO (Della Greca) and NMSS EO (Pierson). | | | | * * * UPDATE ON 07/25/03 AT 0921 EDT FROM JOON PARK TO JOHN MACKINNON * * * | | | | Post-op dosimetry for two patients were determined to be a | | misadministration. The patients had their prostates treated some time in | | the year 2001. The iodine-125 seeds were placed 2 to 3 centimeters below | | the area where they were supposed to be located. The improper location of | | the iodine-125 seeds caused more than 50% of the prescribed dose to be | | delivered to an un-intended organ. The patients will be notified. | | | | Notified R1DO (Dan Holody) and NMSS EO (Trish Holahan). | | | | * * * UPDATE ON 07/30/03 AT 0911 EDT FROM JOON PARK TO ARLON COSTA * * * | | | | Two additional patients of a group of seven were identified as having | | received a misadministration of iodine-125 to an unintended organ. The | | patients will be notified of this misadministration. The licensee is in the | | process of clarifying and document the issues related to this incident. | | | | Notified R1DO (James Moorman) and NMSS EO (Tom Essig). | | | | * * * UPDATE ON 08/07/03 AT 1535 EDT FROM CHARLES LEE TO NATHAN SANFILIPPO * | | * * | | | | Another patient has been identified who received a misadministration of | | iodine-125 to the prostate. The prescribed dose was 144 Gy, and it was | | delivered using 76 seeds and 27 needles as planned prior to the implant | | date. After reviewing the CT, which was done on Feb. 27, 2001, the V100 of | | the prostate received 29% of the prescribed dose. The penile bulb at 72 Gy | | received 44.8%. The licensee indicated that they have looked into 8 | | patients who may have been misadministered, of which, one was not declared a | | misadministration. The other seven appear in this notification. There are | | 23 total patients that the licensee intends to review. | | | | Notified R1DO (Clifford Anderson) and NMSS EO (Fred Brown). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40033 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 07/29/2003| | UNIT: [] [2] [] STATE: AZ |NOTIFICATION TIME: 21:13[EDT]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 07/29/2003| +------------------------------------------------+EVENT TIME: 15:16[MST]| | NRC NOTIFIED BY: DUANE KANITZ |LAST UPDATE DATE: 08/06/2003| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CHUCK CAIN R4 | |10 CFR SECTION: |PAT GWYNN RA | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|WILLIAM BECKNER NRR | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | |ACCS 50.72(b)(2)(iv)(A) ECCS INJECTION | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 98 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 2 WAS MANUALLY TRIPPED AFTER A STUCK OPEN SPRAY VALVE FAILED TO CLOSE | | | | "On July 29, 2003, at approximately 1518 Mountain Standard Time (MST) Palo | | Verde Unit 2 plant operators manually tripped the reactor from approximately | | 98% rated thermal power due to reduced reactor coolant system pressure when | | a pressurizer spray valve opened and failed to close on operator demand. | | Unit 2 was at normal temperature and pressure prior to the trip. All CEAs | | inserted fully into the reactor core. This was an uncomplicated reactor | | trip. No emergency classification was required per the Emergency Plan. | | Containment Isolation and Safety Injection Actuation Signals were received | | following the manual reactor trip per design. Safety related buses remained | | energized during and following the reactor trip. No significant LCOs have | | been entered as a result of this event. The pressurizer spray valve that | | initiated the event was being placed in service following maintenance. | | | | "Unit 2 is stabilized in Mode 3 at approximately 564 degrees F and 2200 | | psia. The reactor coolant system remains in natural circulation with heat | | removal via Steam Bypass Control to the main condenser. The event did not | | result in any challenges to fission product barriers and there were no | | adverse safety consequences as a result of this event. The event did not | | adversely affect the safe operation of the plant or the health and safety of | | the public. | | | | "The Resident Inspector was informed of the Unit 2 reactor trip and this | | notification. The Resident Inspector is onsite to observe response to the | | reactor trip. | | | | "The reactor coolant pumps were secured after the trip to stop continued | | spray flow and depressurization per the alarm response procedure. The | | offsite electrical power grid is stable." | | | | * * * UPDATE ON 8/6/03 AT 2325 EDT FROM D. GRAFF TO E. THOMAS * * * | | | | "At the time of the initial notification it was not believed that an ECCS | | discharge to the RCS occurred. Subsequent review of post-trip data | | determined that injection did occur. The total accumulated actuation cycles | | to date for Palo Verde Unit 2 is 8. The thermal fatigue limit is 160 | | cycles, thus the unit is well within the 0.70 (70%) usage threshold of 112 | | cycles. | | | | "Unit 2 is in Mode 1 at approximately 98% power, normal operating | | temperature and pressure. | | | | "The NRC Resident Inspector has been notified of this followup | | notification." | | | | The ECCS actuation occurred on a low pressurizer pressure signal. | | | | Notified R4DO (J. Whitten) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40049 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 08/06/2003| | UNIT: [] [2] [] STATE: PA |NOTIFICATION TIME: 19:12[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 08/06/2003| +------------------------------------------------+EVENT TIME: 16:30[EDT]| | NRC NOTIFIED BY: GEORGE STOROLIS |LAST UPDATE DATE: 08/06/2003| | HQ OPS OFFICER: BILL GOTT +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CLIFFORD ANDERSON R1 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANALYZED CONDITION | | | | "On 8/06/2003 at 1630 hours, the Beaver Valley Power Station (BVPS) Unit 2 | | control room was notified by Engineering that the manual operator actions | | specified in Unit 2 post-fire procedures are not adequate for defeating a | | potential fire-induced spurious operation of the Power Operated Relief | | Valves (PORVs). The procedure step de-energizes the PORVs by opening | | breakers at the d-c distribution panel. This action alone would not be | | sufficient to prevent a cable-to-cable hot short from re-energizing the | | circuit since the de-energized circuit is routed in cable trays with other | | energized circuits in the affected fire areas. Preliminary reviews have | | identified the following potentially affected fire areas: | | | | CB-1 Control Building Instrumentation and Relay Area | | CB-2 Control Building Cable Spreading Room | | CB-3 Control Building Main Control Room | | CB-6 Control Building West Communication Room | | CT-1 Cable Tunnel | | CV-1 Cable Vault and Rod Control Area | | SB-1 Emergency Switchgear Room (Orange) | | RC-1 Reactor Containment | | | | "An hourly roving fire watch patrol has been established for the affected | | fire areas as compensatory measures, with the exception of the Main Control | | Room and the Reactor Containment area, until the condition is fully | | evaluated and resolved. The Main Control Room is continuously manned and | | does not require an hourly fire watch patrol. The Reactor Containment area | | is not accessible during normal power operations and, as such, compensatory | | measures for this area will include a once-per-shift verification of remote | | instrumentation by operations personnel to confirm that there are no | | abnormal conditions or indications for this area. | | | | "This condition was discovered during the review of manual operator actions | | for fire-induced spurious operations to confirm the safe shutdown circuit | | analysis is consistent with the manual actions identified in the | | procedures. | | | | "This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii) as an | | unanalyzed condition that significantly degraded plant safety since the | | failure to assure the PORVs remain in the closed position could result in | | the failure to meet the fire protection safe shutdown criteria. BVPS Unit 2 | | was licensed to the NUREG 0800 Standard Review Plan 9.5.1 "Fire Protection | | Program", and License Condition 2.F requires compliance to the provisions of | | the approved fire protection program as described in the Final Safety | | Analysis Report. UFSAR Section 9.5A.1.2.1.6 states that the safe shutdown | | capability should not be adversely affected by a fire in any plant area | | which results in spurious actuation of the redundant valves in any one | | high-low pressure interface line. Even though there is a very low | | likelihood of multiple shorts causing a spurious PORV actuation in an | | ungrounded DC circuit, the existing actions to prevent re-energizing the | | circuit and causing a spurious actuation of the PORVs is not consistent with | | the NRC guidance for high-low pressure interface valves. | | | | "The NRC resident inspector has been notified." | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021