Event Notification Report for March 7, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/06/2001 - 03/07/2001 ** EVENT NUMBERS ** 37807 37810 +------------------------------------------------------------------------------+ |Hospital |Event Number: 37807 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SAINT LUKE'S HOSPITAL |NOTIFICATION DATE: 03/05/2001| |LICENSEE: SAINT LUKE'S HOSPITAL |NOTIFICATION TIME: 15:13[EST]| | CITY: KANSAS CITY REGION: 3 |EVENT DATE: 02/23/2001| | COUNTY: STATE: MO |EVENT TIME: 11:15[CST]| |LICENSE#: 24-00889-01 AGREEMENT: N |LAST UPDATE DATE: 03/06/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN MADERA R3 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SCOTT SORENSEN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE MEDICAL MISADMINISTRATION | | | | A remote afterloader device failed to function as it was intended during a | | random FDA trial. The remote afterloader was in automatic, and it was | | supposed to insert an intravascular, brachytherapy, 93-mCi, P-32, wire | | source into a patient. The remote afterloader device did not operate | | properly, and it inserted and withdrew the wire source 4 times. No dwell | | time was recorded by the afterloader since the wire source inserted less | | than 5 seconds each time before the wire source was automatically withdrawn. | | The patient was supposed to have received a total dose of 20 grays. The | | patient received a dose much less than intended. The FDA was notified of | | this event by the licensee. | | | | ***** UPDATE AT 0958 EST ON 03/06/01 FROM SCOTT SORENSEN TO LEIGH TROCINE | | ***** | | | | The licensee called the NRC Operation Center to clarify that the trial | | afterloader device was under the operator's control and that the device's | | internal safety checks and sensors caused the source to be removed and would | | not allow the dose to be delivered as intended. The following text is a | | portion of a clarification received from the licensee via an E-mail at 1024 | | EST on 03/06/01: | | | | "Radiation therapy was not delivered as prescribed during [an] FDA-approved | | clinical trial for Intravascular Brachytherapy. A 93-mCi P-32 wire was to | | be placed across a coronary artery lesion for approximately 5 | | minutes of dwell time. Multiple attempts were made to place the source at | | the treatment position. However, an internal safety trigger in the | | afterloader caused the source wire to be withdrawn from the patient | | immediately upon source arrival at the targeted treatment site. The | | licensee extended the active wire a total of 4 times into the patient, | | followed by immediate, automatic withdrawal by the afterloader. No dwell | | time was recorded at the treatment location, and transit time through the | | patient's arteries was approximately 5 seconds each way. The procedure was | | abandoned without the patient receiving the intended 20 Gray dose. The | | event was under direct supervision of [an] NRC-approved Radiation Oncologist | | and the institution's Radiation Safety Officer. The FDA was notified of the | | study protocol deviation by the licensee." | | | | (Call the NRC operations officer for licensee contact information.) | | | | The NRC operations officer notified the R3DO (Madera) and NMSS EO (Sturz). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37810 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEABROOK REGION: 1 |NOTIFICATION DATE: 03/06/2001| | UNIT: [1] [] [] STATE: NH |NOTIFICATION TIME: 00:24[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 03/05/2001| +------------------------------------------------+EVENT TIME: 23:24[EST]| | NRC NOTIFIED BY: JIM CROWLEY |LAST UPDATE DATE: 03/06/2001| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNU |RICHARD CONTE R1 | |10 CFR SECTION: |BILL BATEMAN NRR | |*AEC 50.72(a) (1) (i) EMERGENCY DECLARED |CHARLES MILLER IRO | |*RPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|CHARLIE BAGWELL FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCRETIONARY UNUSUAL EVENT DECLARED DUE TO A MOMENTARY LOSS OF OFFSITE | | POWER DURING AN ONGOING SEVERE WINTER STORM AND SUBSEQUENT AUTOMATIC REACTOR | | TRIP DUE TO GRID INSTABILITY | | | | During an ongoing severe winter storm, the 345-kV breakers tripped open and | | re-closed resulting in a momentary loss of offsite power. An automatic | | reactor trip also occurred at 2324 on 03/05/01 due to electrical grid | | instability. (The exact cause of the reactor trip is currently under | | investigation because there was no first out indication.) All rods fully | | inserted. The reactor coolant pumps tripped as expected, and one has been | | placed back in service. Both emergency diesel generators automatically | | started but did not load. Availability of the condenser was also lost due | | to the loss of power, and operators closed the main steam isolation valves. | | There were no radiation releases, and there were no reactor coolant system | | or steam generator tube leaks. All systems functioned as required with one | | exception. The steam-driven emergency feedwater pump failed to | | automatically actuate. | | | | At this time, the unit is in Mode 3. Normal charging and letdown, | | pressurizer heaters and sprays, and one reactor coolant pump are being | | utilized for primary system level, pressure, and transport control. Water | | is being supplied to the steam generators via an electric-driven emergency | | feedwater pump, and the atmospheric dumps are being utilized as the heat | | sink. Containment parameters are normal. The grid is currently available | | for offsite power, and the emergency diesel generators are still running. | | | | Based on a discretionary shift management call, the licensee declared an | | Unusual Event at 2336 on 03/05/01. The licensee stated that a | | "Discretionary Event" under item 18A refers to an event in progress (or has | | occurred) that indicates a potential degradation of the level of safety of | | the station. The licensee plans to notify the NRC when the Unusual Event | | has terminated or if conditions degrade. | | | | A severe winter storm is currently ongoing. At the time of the event, the | | unit was experiencing winds at a rate of approximately 50 miles per hour. | | The licensee reported that these strong winds were ongoing and that only a | | few inches of snow had fallen (although up to 2 feet is expected). | | | | The licensee notified the state at 2347 on 03/05/01 and plans to notify the | | NRC resident inspector as well as applicable local officials. The licensee | | also plans to issue a press release. | | | | ***** UPDATE AT 0222 ON 03/06/01 FROM JIM HILL TO LEIGH TROCINE ***** | | | | This update provides both clarifications/corrections to the original event | | notification and additional information regarding licensee plans. | | | | CLARIFICATIONS/CORRECTIONS: Prior to the event, two of three offsite power | | lines had been lost in close succession. The remaining offsite line was | | subsequently lost, and its breaker re-closed within a short duration. This | | resulted in the momentary loss of offsite power and subsequent plant | | transient. This initial electrical imbalance was sufficient to result in | | the automatic starting and loading of both emergency diesel generators. | | | | CURRENT STATUS: The unit remains in the Unusual Event, and winds are | | currently sustained at a rate of approximately 40 miles per hour. All three | | offsite power lines have been restored. Both emergency diesel generators | | remain in operation and continue to provide power to both vital (emergency) | | buses. The non-vital buses have been re-energized from offsite power. An | | additional auxiliary pump (the startup feedwater pump) has also been started | | to provide additional water to the steam generators. This pump is a | | non-safety related housekeeping pump. | | | | PLANS: Within the next half hour, the licensee plans to commence a | | discretionary plant cooldown and plans to place the unit in Mode 5 (Cold | | Shutdown). At some point in time, the licensee also plans to secure the | | electric-driven emergency feedwater pump and rely on the startup feedwater | | pump to supply water to the steam generators. | | | | The licensee notified the NRC resident inspector and an onsite member of an | | NRC residual heat removal inspection team. The NRC operations officer | | notified the R1DO (Conte), NRR EO (Bateman), and IRO (Miller). | | | | ***** UPDATE AT 0438 ON 03/06/01 FROM JIM HILL TO LEIGH TROCINE ***** | | | | The licensee has commenced a plant cooldown and anticipates that it will | | take approximately 6 hours for the unit to reach Cold Shutdown. Other than | | commencement of the cooldown, there has been no change in plant conditions | | or equipment status. | | | | The licensee stated that the criteria for exiting the Unusual Event have | | been met. However, the licensee currently plans to remain in the Unusual | | Event for a while longer because the high line insulators onsite are still | | arcing and are suspect and because the in-house vital buses are still being | | powered by the emergency diesel generators. | | | | The licensee notified an onsite member of an NRC residual heat removal | | inspection team, who in turn notified the NRC resident inspector. The NRC | | operations officer notified the R1DO (Conte), NRR EO (Bateman), and IRO | | (Miller). | | | | ***** UPDATE AT 0800 ON 03/06/01 FROM JOHN LaVALLEY TO LEIGH TROCINE ***** | | | | The licensee called to provide the following status update: | | | | The unit remains in the Unusual Event. The reactor coolant system is | | currently at 445 degrees F, and the cooldown is still in progress via | | utilization of boration and the atmospheric steam dumps. The emergency | | diesel generators are still supplying power to the vital buses. | | | | The licensee currently plans to place the unit in Mode 5 (Cold Shutdown) and | | then to restore the secondary side of the plant (assuming that offsite power | | supplies are stable). | | | | The NRC operations officer notified the R1DO (Conte) and NRR EO (Tappert). | | | | *** UPDATE AT 1509 ET ON 03/06/01 FROM JOHN LaVALLEY TO JOHN MACKINNON | | ***** | | | | The licensee called to provide the following status update: | | | | The unit remains in the Unusual Event. The reactor coolant system is | | currently 360 degrees F, and cooldown is still in progress. The licensee | | will reduce reactor coolant system temperature to approximately 240 degrees | | F. The emergency diesel generators are still supplying power to the vital | | buses. The licensee is waiting for Load Dispatcher permission to take down | | one 345kV line at a time to clean the lines bushing. After the bushings for | | the 3 345kV lines have been cleaned and the grid is stable, the licensee | | will make a determination whether to exit the Unusual Event. | | Additional information: After the reactor trip the Turbine Driven Auxiliary | | Feedwater pump failed to start. The licensee thinks that the pump tripped | | on overspeed. Licensee is investigating this problem. | | | | The NRC operations officer notified the R1DO (Bellamy) and NRR EO (C. | | Grimes) | | | | ****UPDATE AT 1619ET ON 03/06/01 FROM M KILEY TO JOHN MACKINNON***** | | | | The licensee called to provide the following clarification to event write | | up: | | | | The exact cause of the reactor trip as indicated by the "First Out Light" | | was "Power Range Negative Flux Rate Hi". Secondly, both Emergency Diesel | | Generators automatically started and loaded all safety related loads | | associated with Emergency Electrical Buses 5 and 6. | | | | The NRC operations officer notified the R1DO (Bellamy) and NRR EO (Tad | | Marsh). | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021