Event Notification Report for June 16, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/15/2000 - 06/16/2000 ** EVENT NUMBERS ** 37084 37085 37086 37087 37088 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37084 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 06/15/2000| | UNIT: [1] [2] [] STATE: NC |NOTIFICATION TIME: 07:51[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 06/15/2000| +------------------------------------------------+EVENT TIME: 06:57[EDT]| | NRC NOTIFIED BY: JOE COSTA |LAST UPDATE DATE: 06/15/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RUDOLPH BERNHARD R2 | |10 CFR SECTION: | | |AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF NINE EMERGENCY OFFSITE SIRENS DUE TO LOSS OF LOCAL POWER | | | | The licensee was notified that at 0657 EDT that nine of the offsite | | emergency warning sirens were deenergized at 0408 EDT due to local power | | outage and were inoperable for greater than one hour. Six were restored in | | 1 hour and 16 minutes and the other three were restored in 2 hours and 16 | | minutes. All sirens are now operable. | | | | The licensee notified the NRC Resident Inspector and the State authorities. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37085 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 06/15/2000| |LICENSEE: PROFESSIONAL SERVICE INDUSTRIES INC |NOTIFICATION TIME: 10:25[EDT]| | CITY: TAMPA REGION: 2 |EVENT DATE: 06/14/2000| | COUNTY: STATE: FL |EVENT TIME: 09:00[EDT]| |LICENSE#: 22-12 AGREEMENT: Y |LAST UPDATE DATE: 06/15/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |RUDOLPH BERNHARD R2 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLES ADAMS (FACSIMILE) | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT | | | | The State of Florida Bureau of Radiation Control reported that a Troxler | | soil moisture/density gauge (Model 3430, Serial #30059), containing 8 mCi of | | Cs-137 and 40 mCi of Am-241/Be, had been stolen from a state licensee. The | | licensee reported that the gauge was stolen from a temporary job site | | between the hours of 6 p.m. on 6/13/00 and 9 a.m. on 6/14/00. The chain link | | fence surrounding the site was not damaged, but the door to the shed had | | been pried open. The lock on the storage locker containing the container and | | gauge had been cut. The gauge and container were the only items taken. The | | Hillsborough Sheriff's Office and the Florida Bureau of Radiation Control | | are investigating. The Sheriff's Office is planning to issue a press | | release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Hospital |Event Number: 37086 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SIOUX VALLEY HOSPITAL |NOTIFICATION DATE: 06/15/2000| |LICENSEE: SIOUX VALLEY HOSPITAL |NOTIFICATION TIME: 13:52[EDT]| | CITY: SIOUX FALLS REGION: 4 |EVENT DATE: 04/04/2000| | COUNTY: STATE: SD |EVENT TIME: 12:30[MDT]| |LICENSE#: 40-12378-01 AGREEMENT: N |LAST UPDATE DATE: 06/15/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LINDA SMITH R4 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DOUG WARNER | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |LADM 35.33(a) MED MISADMINISTRATION | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PATIENT DID NOT RECEIVE THERAPEUTIC DOSE OF I-131 AS PRESCRIBED | | | | On 4/4/2000 at 1230 hours a patient undergoing treatment for thyroid cancer | | did not receive the 100 mCi of I-131 as stated in the written instructions. | | The Patient Appointment Center misinterpreted the instruction "100mCi I-131 | | followed by a whole body scan" to mean "I-131 whole body scan." A | | diagnostic administration of 4.26 mCi I-131 was given for the whole body | | scan. The whole body scan results were reviewed and the prescribing | | physician concluded that the therapeutic dose was not required. The patient | | was informed. The Heath Physicist consultant to the hospital reviewed the | | incident and advised the hospital that the error was recordable but not | | reportable. This report is being made following an inspection by NRC Region | | 4 (J. Cruz). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37087 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 06/15/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 21:54[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 06/15/2000| +------------------------------------------------+EVENT TIME: 19:15[CDT]| | NRC NOTIFIED BY: MARSHALL FUNKHOUSER |LAST UPDATE DATE: 06/15/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |DAVID HILLS R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE CORE SPRAY (HPCS) DECLARED INOPERABLE DUE TO INCOMPLETE POST | | MODIFICATION TESTING OF IT'S ASSOCIATED DIESEL GENERATOR | | | | "At 1915 on 6/15/00 a Engineering review of a plant modification to the | | Division 3 Diesel Generator (DG) determined that the Post Modification | | Testing did not verify proper operation of the Loss of Off-Site Power (LOOP) | | circuitry. This modification had only been performed to Division 3 DG and | | therefore Division 1 and 2 DG's are not affected. Division 3 DG provides | | power to the High Pressure Core Spray (HPCS) pump. The failure of Division 3 | | DG to operate during a LOOP would have prevented HPCS from operating. The | | loss of a single train safety system such as HPCS is reportable under | | 10CFR50.72(b)(2)(iii)(D)." | | | | The plant modification involved rewiring the electrical circuit to correct | | for a degraded voltage condition and was completed on 1/24/99. Post | | modification testing was completed on 1/31/99. HPCS has been declared | | inoperable but is available, if needed, pending completion of additional | | testing. The licensee will inform the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37088 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUMMER REGION: 2 |NOTIFICATION DATE: 06/15/2000| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 22:10[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 06/15/2000| +------------------------------------------------+EVENT TIME: 21:37[EDT]| | NRC NOTIFIED BY: DAN GOLDSTON |LAST UPDATE DATE: 06/15/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RUDOLPH BERNHARD R2 | |10 CFR SECTION: | | |ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT COMMENCED A CONTROLLED TECH SPEC REQUIRED SHUTDOWN TO MODE 2 FOR | | REPAIRS | | | | "The 'C' steam generator Feedwater Isolation Valve, XVG1611C, air operator | | developed an air leak and was declared inoperable 6/13/00 at 1549EDT. | | Efforts to stop the leak were unsuccessful. At 2137EDT on 6/15/00 a | | controlled power reduction to mode 2 was started. Current plans are to | | repair the operator in mode 2 and return to power operation." | | | | The air leak is ongoing with the affected valve in use (open). The licensee | | anticipates entering mode 2 by 0600EDT on 6/16/00 and has informed the NRC | | Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021