Event Notification Report for March 28, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/27/2000 - 03/28/2000 ** EVENT NUMBERS ** 36771 36817 36836 36837 36838 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36771 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 03/08/2000| | UNIT: [1] [] [] STATE: TX |NOTIFICATION TIME: 12:18[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/07/2000| +------------------------------------------------+EVENT TIME: 13:00[CST]| | NRC NOTIFIED BY: MARILYN JOHNSON |LAST UPDATE DATE: 03/27/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KRISS KENNEDY R4 | |10 CFR SECTION: | | |NLTR LICENSEE 24 HR REPORT | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR CONDITION OF LICENSE REPORT INVOLVING TECH SPEC REQUIREMENTS | | | | "On February 9, 2000, it was discovered that the Flux Multiplication Alarm | | (which is used to mitigate boron dilution accidents) was not functional. It | | was not recognized at that time that this caused the associated extended | | range neutron detector to be inoperable. If an extended range detector is | | inoperable in Modes 3, 4, and 5 the Technical Specifications requires that | | operations be suspended involving positive reactivity changes. | | | | "On March 1, 2000 at 0017 hours Unit 1 entered Mode 3 as part of a shutdown | | to support refueling activities. | | Immediately following Mode 3 entry testing was performed which involves | | raising control rods to perform drop | | testing. Raising control rods constitutes positive reactivity which is | | contrary to requirements of the Technical | | Specifications. | | | | "This notification is being made pursuant to Operating License NPF-76 | | Condition 2.G for operation or condition prohibited by Technical | | Specifications." | | | | The licensee will inform the NRC resident inspector. | | | | * * * UPDATE AT 1417 ON 03/27/00 BY KEN TAPLETT TO JOLLIFFE * * * | | | | Further licensee review determined that the extended range neutron detector | | in question had been operable during the positive reactivity change | | activity. During the time of the original notification, the Flux | | Multiplication Alarm was thought to be non-functional. A non-functional | | Flux Multiplication Alarm causes the associated extended range neutron | | detector to be inoperable. It was determined that the Flux Multiplication | | Alarm was actually functional at the completion of surveillance testing | | conducted on February 9, 2000. The surveillance procedure requires an alarm | | reset prior to exiting the surveillance test which arms the Flux | | Multiplication Alarm circuit thus making it functional. Although this step | | was performed on February 9, 2000, the performers did not recognize at the | | time that this corrected the perceived loss of alarm function. | | | | Prior to the February 9, 2000 surveillance test, the last satisfactory | | performance of the Flux Multiplication Alarm surveillance was conducted on | | November 16, 1999 with a grace period to March 10, 2000. Unit 1 entered | | Mode 6 (where the requirement was no longer applicable) on March 3, 2000 and | | has remained in that mode for a refueling and steam generator replacement | | outage. A satisfactory surveillance test was conducted on March 16, 2000. | | | | The licensee plans to revise the test procedure to preclude recurrence of | | this event. | | | | Based upon the above justification, the licensee desires to retract this | | event. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R4DO Kriss Kennedy. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36817 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: RIVER BEND REGION: 4 |NOTIFICATION DATE: 03/20/2000| | UNIT: [1] [] [] STATE: LA |NOTIFICATION TIME: 17:03[EST]| | RXTYPE: [1] GE-6 |EVENT DATE: 03/20/2000| +------------------------------------------------+EVENT TIME: 15:05[CST]| | NRC NOTIFIED BY: TOM LYNCH |LAST UPDATE DATE: 03/27/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LAWRENCE YANDELL R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECURITY REPORT | | | | A contact employee attempted to bring contraband into the Protected Area. | | Immediate compensatory actions were taken upon discovery. The licensee | | notified the NRC resident inspector. Contact the NRC Operations Center for | | additional details. | | | | * * * UPDATE AT 1513 ON 03/27/00 FROM KIM AITKEN TO JOLLIFFE * * * | | | | Further licensee investigation revealed that there was no significant threat | | to River Bend Station or the public and that the vendor employee had no | | malevolent intent. After review of Reg Guide 5.62, NUREG 1304, and Generic | | Letter 91-03, the licensee has determined that this event is not reportable | | under 10CFR26, 10CFR50.72, 10CFR73.71, or 10CFR73, Appendix G.l.d criteria | | and thus, the licensee desires to retract this event. The licensee has | | discussed this event with Region IV security personnel and the NRC Resident | | Inspector. The NRC Operations Officer notified the R4DO Kriss Kennedy. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36836 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HATCH REGION: 2 |NOTIFICATION DATE: 03/27/2000| | UNIT: [] [2] [] STATE: GA |NOTIFICATION TIME: 09:17[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/27/2000| +------------------------------------------------+EVENT TIME: 08:00[EST]| | NRC NOTIFIED BY: URQUHART |LAST UPDATE DATE: 03/27/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF LOCAL LEAK RATE TEST. | | | | DURING LOCAL LEAK RATE TESTING(LLRT) OF THE "2G11-F004", DRYWELL FLOOR DRAIN | | SUMP PRIMARY CONTAINMENT ISOLATION VALVE, IT WAS DETERMINED THAT THE VALVE | | LEAKS AT A RATE GREATER THAN 30,000 ACCM(ACTUAL CUBIC CENTIMETERS/MIN) WHICH | | IS GREATER THAN THE PROCEDURAL LIMITS. THIS IN COMBINATION WITH ITS | | COMPANION( IN SERIES) ISOLATION VALVE(2G11-F003) WHICH HAD FAILED A PREVIOUS | | LLRT AND WAS REPAIRED, BUT FAILED ITS RETEST, RESULTED IN THE TECH SPEC | | LIMIT FOR 0.009L-SUB-A BEING EXCEEDED FOR BYPASS LEAKAGE. THE TEST WAS | | PERFORMED ON 3/26 AND WAS EVALUATED THIS MORNING. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 36837 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FLORIDA BUREAU OF RADIATION CONTROL |NOTIFICATION DATE: 03/27/2000| |LICENSEE: DUNKELBERGER ENGINEERING & TESTING |NOTIFICATION TIME: 10:00[EST]| | CITY: WEST PALM BEACH REGION: 2 |EVENT DATE: 03/27/2000| | COUNTY: PALM BEACH STATE: FL |EVENT TIME: [EST]| |LICENSE#: 2462-2 (FL) AGREEMENT: Y |LAST UPDATE DATE: 03/27/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |THOMAS DECKER R2 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: CHARLEY E. ADAMS (FL) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT INVOLVING RECOVERED TROXLER GAUGE | | | | "Citizen found troxler gauge [containing 8mCi Cs-137 and 40mCi Am-241:Be] | | along road and took it to the Royal Palm Beach PD. Owner notified this | | office of missing gauge, was told of it's location [Intersection of 41 & 67 | | in Royal Palm Beach], and then took possession. There was no damage to the | | gauge which was in a locked case. Owner said that the operator failed to | | secure the gauge to the truck when leaving a work site. Florida is | | investigating the incident [Florida Incident #FL00-054]." | | | | The licensee lost the device on the morning of 3/27/00 when it fell off his | | truck due to not being properly secured. | | | | Call the Headquarters Operations Center for contact information. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36838 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 03/27/2000| | UNIT: [1] [2] [] STATE: TN |NOTIFICATION TIME: 14:43[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/27/2000| +------------------------------------------------+EVENT TIME: 10:08[EST]| | NRC NOTIFIED BY: TERRY KNUETTEL |LAST UPDATE DATE: 03/27/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |THOMAS DECKER R2 | |10 CFR SECTION: | | |HFIT 26.73 FITNESS FOR DUTY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FITNESS FOR DUTY EVENT - | | | | A temporary employee foreman tested positive for illegal drugs during a | | random drug test. The licensee terminated the employee's plant access | | authorization. Contact the NRC Operations Officer for additional details. | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021