Event Notification Report for March 22, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/21/2000 - 03/22/2000 ** EVENT NUMBERS ** 36812 36815 36819 36820 36821 36822 36823 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36812 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRUNSWICK REGION: 2 |NOTIFICATION DATE: 03/19/2000| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 23:31[EST]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/19/2000| +------------------------------------------------+EVENT TIME: 20:00[EST]| | NRC NOTIFIED BY: MARK SCHALL |LAST UPDATE DATE: 03/21/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY OF REACTOR COOLANT SYSTEM LEAKAGE ON THE WITHDRAWAL LINE WELDS OF | | THREE CONTROL ROD DRIVE MECHANISMS DURING HYDRO TESTING | | | | The following text is a portion of a facsimile received from the licensee: | | | | "EVENT: During [the performance of procedure] OPT-80. 1, Reactor Pressure | | Vessel ASME Vessel ASME Section XI Pressure Test, reactor coolant system | | (RCS) pressure boundary leakage was observed on the withdrawal line welds of | | three control rod drive mechanisms (CRDM). The following CRDMS were noted | | with leakage: CRDM 06-15 (10 drops/minute at 1030 psig), CRDM 30-15 (20 | | drops/minute at 1030 psig) and CRDM 14-19 (20 drops/minute at 1030 psig). | | This leakage is outside the acceptance standard of zero leakage per ASME | | Section XI, Table IWB-3410-1." | | | | "INITIAL SAFETY SIGNIFICANCE EVALUATION: Minimal; the leakage is well | | within the capacity of available injection systems." | | | | "CORRECTIVE ACTION(S): The CRDMs will be removed, and the affected areas | | repaired prior to reactor startup." | | | | The licensee notified the NRC resident inspector. | | | | * * * RETRACTION 1522 3/21/2000 FROM MARK TURKAL TAKEN BY BOB STRANSKY * * | | * | | | | "Upon further inspection and evaluation, CP&L had determined that the | | previously reported leaks from control rod drive mechanisms (CRDMs) 06-15, | | 30-15, and 14-19 do not represent a serious degradation of a principal | | safety barrier. | | | | "Based on the location of the leaks, it was conservatively assumed to be | | pressure boundary leakage coming from the withdrawal line welds to the CRD | | housing flange; which was outside the acceptance criteria of zero leakage | | per ASME Section XI, Table IWB-3410-1. CP&L notified the NRC at 23:31 EST | | (i.e., Event Number 36812), in accordance with 10 CFR 50.72(b)(2)(i), that a | | condition on Unit 1 had been identified that had it been found while the | | reactor was in operation, would have resulted in the nuclear power plant, | | including its principal safety barriers, being seriously degraded. | | | | "Subsequently, repressuization of the Unit 1 reactor pressure vessel was | | performed and the leaks were observed using advanced video inspection | | techniques. Based on this re-inspection, it was determined, on March 21, | | 2000, that the leakage was from the CRDM flange bolting and not the | | withdrawal line welds. As such, this is not pressure boundary leakage and | | the zero leakage acceptance criteria of ASME Section XI, Table IWB-3410-1 is | | not applicable. This condition does not represent a serious degradation of a | | principal safety barrier. | | | | "CP&L has evaluated and dispositioned the observed leakage, in accordance | | with Code Case N-566-1, 'Corrective Action For Leakage Identified at Bolted | | Connections,' and determined it to be insignificant leakage, which is | | expected to seal during plant heatup." | | | | The NRC resident inspector has been informed of this retraction. Notified | | R2DO (Decker). | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Hospital |Event Number: 36815 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: CARDIOLOGY ASSOC OF FAIRFIELD CO. |NOTIFICATION DATE: 03/20/2000| |LICENSEE: CARDIOLOGY ASSOCIATES OF FAIRFIELD CO|NOTIFICATION TIME: 09:44[EST]| | CITY: NORWALK REGION: 1 |EVENT DATE: 03/20/2000| | COUNTY: STATE: CT |EVENT TIME: [EST]| |LICENSE#: 06-077795-01 AGREEMENT: N |LAST UPDATE DATE: 03/21/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |LAURIE PELUSO R1 | | |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: STUART KORCHIN | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAAA 20.1906(d) SURFACE CONT/ EXT RAD | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EXTERNAL RADIATION LEVELS EXCEEDING THE LIMITS OF 10 CFR 71.47 | | | | CARDIOLOGY ASSOCIATES OF FAIRFIELD COUNTY LOCATED AT 40 CROSS STREET IN | | NORWLAK, CT, RECEIVED A PACKAGE FROM SYNCOR INTERNATIONAL IN STAMFORD, CT, | | LABELED WHITE I WHICH MEASURED 40 mR/HR (EXTERIOR SWIPE READ 38 DPM). THIS | | EXCEEDS THE EXTERNAL RADIATION LEVELS ALLOWED FOR WHITE I. THE PACKAGE | | CONTAINED SEVERAL LEAD PIGS OF TECHNETIUM-99m , ONE OF WHICH WAS | | CONTAMINATED READING 5652 DPM USING A SWIPE. THE LICENSEE NOTIFIED THE | | SYNCOR INTERNATIONAL AND THE NRC REGION I OFFICE (SHANBAKY). | | | | * * * UPDATE 1116EST ON 3/21/00 BY S.SANDIN * * * | | | | THE LICENSEE IS RETRACTING THIS REPORT AFTER FURTHER REVIEW AND DISCUSSIONS | | WITH REGION I (DARDEN). NOTIFIED R1DO (MANNING). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36819 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SEQUOYAH REGION: 2 |NOTIFICATION DATE: 03/21/2000| | UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 06:15[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/21/2000| +------------------------------------------------+EVENT TIME: 04:40[EST]| | NRC NOTIFIED BY: BILL HARRIS |LAST UPDATE DATE: 03/21/2000| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 75 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TURBINE TRIP - REACTOR TRIP | | | | An electrical fault on the main generator caused a turbine trip and an | | anticipatory reactor trip. All rods fully inserted and the plant response | | to the trip was as expected. Decay heat is being removed by dumping steam | | to the main condenser. Auxiliary Feedwater started as expected. Reactor | | coolant pumps are running. Offsite power and the emergency diesel | | generators are operable. | | | | The licensee is investigating the cause of the turbine trip. The licensee | | notified the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36820 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HADDAM NECK REGION: 1 |NOTIFICATION DATE: 03/21/2000| | UNIT: [1] [] [] STATE: CT |NOTIFICATION TIME: 09:48[EST]| | RXTYPE: [1] W-4-LP |EVENT DATE: 03/21/2000| +------------------------------------------------+EVENT TIME: 08:50[EST]| | NRC NOTIFIED BY: JON BOWER |LAST UPDATE DATE: 03/21/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LOUIS MANNING R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Decommissioned |0 Decommissioned | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION INVOLVING MINOR OIL RELEASE TO DISCHARGE CANAL | | | | During demolition of a building, a hydraulic line was severed causing an | | approximate 1-2 gallon spill of oil. A small portion of the spill reached | | the discharge canal creating a sheen on the water. The licensee notified | | the State of Connecticut Department of Environmental Protection (DEP), the | | USCG and the National Response Center (NRC). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36821 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 03/21/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 16:44[EST]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 03/21/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 13:50[CST]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 03/21/2000| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |GEOFFREY WRIGHT R3 | | DOCKET: 0707001 |LARRY CAMPER NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: PITTMAN | | | HQ OPS OFFICER: BOB STRANSKY | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 4-HOUR NRC BULLETIN 91-01 REPORT | | | | "Valves being dispositioned as part of the transfer of material storage | | areas from DOE to USEC in C-331 were incorrectly handled as NCS exempt | | equipment in violation of NCSA GEN-20. NCSA GEN-20 requires that the | | equipment be characterized prior to movement/transportation. Valves located | | in former DMSAs were incorrectly labeled as exempt from NCS controls based | | on invalid assay smear results. The smears contained less than a measurable | | quantity of uranium and valid assay results could not be obtained. Assay | | smears with uranium below a measurable quantity cannot provide an accurate | | measurement of assay. The smear analysis results were incorrectly used to | | determine that the equipment assay was below 1%. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | | | "Assay smears taken to determine the assay of the valves did not contain | | sufficient uranium for analysis. The smears included valve internal | | surfaces, but all internal surfaces were not visible. The items have been | | decontaminated and holdup of uranium in the internal surfaces is highly | | unlikely. In addition, many of the equipment items were not used in UF6 | | service, however, the assay exemption process is not allowed unless valid | | sample analysis results can be obtained. | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO(S) OF HOW | | CRITICALITY COULD OCCUR: | | | | "In order for criticality to be possible, the accumulation of fissile | | material involving an unsafe mass and geometry would have to occur. A | | significant amount of uranium is not believed to be present but no valid | | quantification of mass has been made. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY CONCENTRATION ETC.): | | Double contingency for this scenario is established by implementing two | | independent controls on assay. | | | | "ESTIMATED AMOUNT, ENRICHMENT FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE CRITCAL MASS): | | | | "Unknown due to DOE previously controlling areas. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | | | "No NCS controls (other than providing 10 foot buffer zone) were in place. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS | | IMPLEMENTED: | | | | "All equipment which has been improperly characterized will be identified | | and characterized with proper independent verification of assay and mass. | | The issue of inadequate procedures and/or training for the performance of | | independent assay verification will be corrected by retraining of personnel | | and/or revision of the applicable procedure prior to the performance of any | | further independent assay verifications." | | | | The NRC resident inspector has been notified of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36822 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 03/21/2000| | UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 23:12[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 03/21/2000| +------------------------------------------------+EVENT TIME: 18:50[CST]| | NRC NOTIFIED BY: GUNDERSON |LAST UPDATE DATE: 03/21/2000| | HQ OPS OFFICER: BOB STRANSKY +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEOFFREY WRIGHT R3 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM INOPERABLE | | | | "During performance of Unit One HPCI System Logic Functional Test, the HPCI | | Auxiliary oil pump would not stay running and the turbine stop valve did not | | open on receipt of a simulated auto initiation signal. The Auxiliary oil | | pump was subsequently taken to manual, at which time the pump stayed running | | and the turbine stop valve opened. HPCI is inoperable with Engineering and | | Maintenance troubleshooting possible pressure switch problems." | | | | The NRC resident inspector has been informed of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36823 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 03/22/2000| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 00:48[EST]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 03/21/2000| +------------------------------------------------+EVENT TIME: 21:36[EST]| | NRC NOTIFIED BY: STEVE FREGEAU |LAST UPDATE DATE: 03/22/2000| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LOUIS MANNING R1 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - SERVICE WATER SYSTEM NONESSENTIAL VALVES ISOLATED DURING MAINTENANCE | | ACTIVITIES - | | | | During performance of preplanned Division I Service Water System (SWS) logic | | circuitry relay replacement activities, an installed electrical jumper | | failed to maintain contact within the circuit causing a fuse to blow and the | | subsequent automatic isolation of the Division II SWS nonessential valves. | | This potential failure had been discussed in preevaluation briefings as a | | distinct possibility and a contingency was in place. | | | | Maintenance technicians replaced the fuse and restored flow to the | | nonessential headers. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021