Event Notification Report for October 22, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/21/1999 - 10/22/1999 ** EVENT NUMBERS ** 35183 35790 36079 36255 36325 36326 36327 36328 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35183 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 12/21/1998| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 19:16[EST]| | RXTYPE: [1] GE-4 |EVENT DATE: 12/21/1998| +------------------------------------------------+EVENT TIME: 16:20[EST]| | NRC NOTIFIED BY: PETE ABBOTT |LAST UPDATE DATE: 10/21/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JOHN WHITE R1 | |10 CFR SECTION: | | |AINB 50.72(b)(2)(iii)(B) POT RHR INOP | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 25 Power Operation |25 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | -HIGH PRESSURE COOLANT INJECTION SYSTEM INOPERABLE DUE TO SYSTEM FLOW | | OSCILLATIONS- | | | | WHILE TESTING THE HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM AT 25% | | POWER, THE LICENSEE OBSERVED SYSTEM FLOW OSCILLATIONS. THE LICENSEE REMOVED | | THE HPCI TURBINE FROM SERVICE TO DETERMINE THE CAUSE AND TAKE CORRECTIVE | | ACTIONS AND DECLARED THE HPCI SYSTEM INOPERABLE. TECH SPEC LCO A/S | | 3.5.C.1.a REQUIRES THE LICENSEE TO RESTORE THE HPCI SYSTEM TO OPERABLE | | STATUS WITHIN 7 DAYS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | * * * UPDATE AT 1332 ON 10/21/99 BY BOB STEIGERWELD TO JOLLIFFE * * * | | | | This notification retracts an earlier report made at 1916 on 12/21/98 per | | 10CFR50.72(b)(2)(iii)(B) and (D), due to observed flow oscillations during | | HPCI System testing. On 12/23/98, the licensee determined that the flow | | oscillation did not affect the operability of the HPCI System and this event | | notification should have been retracted at that time. | | | | During HPCI System testing following a refueling outage, the HPCI System was | | declared inoperable due to observed flow spiking indication on start up of | | the system. Upon further investigation, the observed oscillations were | | attributed to spiking on system startup due to either air in the flow | | transmitter or electronic noise providing a false momentary indication. In | | either case, it was demonstrated that the HPCI System was not affected by | | the momentary spiking indication and the system was able to perform its | | function and was determined to be operable. Therefore, this event | | notification is being retracted. | | | | The licensee notified the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO Bill Cook. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35790 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/03/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:44[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/02/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:30[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 10/21/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |DAVID HILLS R3 | | DOCKET: 0707001 |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: THOMAS WHITE | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THREE SPRINKLER SYSTEMS DECLARED INOPERABLE DUE TO CORRODED HEADS (24-hour | | report) | | | | The following text is a portion of a facsimile received from Paducah: | | | | "On 06/02/99 at 1630 CDT, the Plant Shift Superintendent (PSS) was notified | | that numerous sprinkler heads were corroded, affecting 16 sprinkler systems | | in C-337 and one system in C-333, such that the ability of the sprinklers to | | flow sufficient water was called into question. Subsequently, these | | sprinkler systems were declared inoperable, and TSR-required actions | | establishing roving fire patrols were initiated. This deficiency was | | detected during scheduled system inspections conducted by Fire Protection | | personnel. Currently, functionality of the sprinkler heads has not been | | fully evaluated by Fire Protection personnel, and the remaining cascade | | buildings are currently being inspected, and if necessary, this report will | | be updated to identify any additional areas. | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | The NRC resident inspector has been notified of this event. | | | | | | * * * UPDATE AT 1022 EDT ON 06/04/99 FROM CAGE TO TROCINE * * * | | | | "Two sprinkler heads on system D-1 in C-337 and two sprinkler heads on | | system 27 in C-335 were identified to also be corroded. These were | | identified to the PSS on 06/03/99 at 1600 CDT and 1601 CDT, respectively, | | and determined to require an update to this report by the PSS. | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | Paducah personnel notified the NRC resident inspector of this update. The | | NRC operations officer notified the R3DO (Hills) and NMSS EO (Combs). | | | | * * * UPDATE AT 2152 EDT ON 06/17/99 FROM WALKER TO POERTNER * * * | | | | "Three sprinkler heads on system C-15 and five sprinkler heads on system B-8 | | in C-333 were identified to also be corroded. The PSS was notified of this | | condition at 1300 CDT on 06/17/99 and determined that an update to this | | report was required." | | | | "It has been determined that this event is reportable under | | 10CFR76.120(c)(2) as an event in which equipment is disabled or fails to | | function as designed." | | | | Paducah personnel notified the NRC resident inspector of this update. The | | NRC operations officer notified the R3DO (Madera). | | | | * * * UPDATE 1440 EDT 6/18/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system C-15 and one sprinkler head on system B-8 in | | C-333 were identified to have corrosion. The PSS was notified of this | | condition at 1350 CDT on 06/18/99. The area of the fire patrol for system | | C-15 was expanded to include the two heads identified as corroded. The one | | head on system B-8 was in the area already being patrolled. The PSS | | determined that an update to this report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Madera). | | | | * * * UPDATE 1315 EDT 6/25/1999 FROM WALKER TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on system D-8 and three sprinkler heads on system D-7 | | in C-337 were identified to have corrosion. The PSS was notified of the | | condition on system D-8 at 0125 CDT on 06/25/99 and at 1019 CDT on 06/25/99 | | for system D-7. Both systems were immediately declared inoperable and LCO | | fire patrol actions were implemented. It was determined that an update to | | this report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Jordan). | | | | * * * UPDATE 2119 EDT 7/30/1999 FROM CAGE TAKEN BY STRANSKY * * * | | | | "Five sprinkler heads and one sprinkler piping tee on C-337 system D-7 were | | identified to have corrosion. The PSS was notified of these corroded system | | parts and declared the system inoperable at 0931 CDT on 07/30/99. LCO | | required fire patrols of the affected area were initiated. The PSS | | determined that an update to this event report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Wright). | | | | * * * UPDATE 1655 EDT 7/31/1999 FROM WHITE TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on C-337 System D-1 were identified to have corrosion. | | The PSS was notified of these corroded system parts and declared the system | | inoperable at 1155 CDT on 7/31/99. LCO required fire patrols of the | | affected area were initiated. The PSS determined that an update to this | | report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Wright). | | | | * * * UPDATE 1546 EDT 8/10/1999 FROM WHITE TAKEN BY STRANSKY * * * | | | | "Two sprinkler heads on C-337 system C-15 were identified to have corrosion. | | The PSS was notified of these corroded system parts and declared the system | | inoperable at 1130 CDT on 8/10/99. LCO required fire patrols of the | | affected area were initiated. The PSS determined that an update to this | | report was required." | | | | The NRC resident inspector has been informed of this update. Notified R3DO | | (Burgess). | | | | * * * UPDATE AT 1154 EDT 8/22/99 FROM WALKER TO POERTNER * * * | | | | Four adjacent sprinkler heads on C-333 System B-1 were identified to have | | corrosion. The PSS was notified of the corroded system parts and declared | | the system inoperable at 0918 CDT on 8/22/99. LCO required fire patrols | | were initiated. The PSS determined that an update to this report was | | required. | | | | It has been determined that this event is reportable under 10CFR76.120(c)(2) | | as an event in which equipment is disabled or fails to function as | | designed. | | | | The NRC resident inspector will be notified. | | | | The NRC operations officer notified the R3DO (Clayton). | | | | * * * UPDATE 2015 EDT ON 8/28/99 FROM W.F. GAGE TO S. SANDIN * * * | | | | The following information was provided as an update to this report: | | | | "Two adjacent sprinkler heads on C-337 System D-11 were identified to have | | corrosion. The PSS was notified of these corroded system parts and declared | | the system inoperable at 1420 [CDT] on 8/28/99. LCO required fire patrols | | of the affected area were initiated. The PSS determined that an update to | | this report was required." | | | | Paducah personnel informed the NRC resident inspector. The NRC operations | | officer notified the R3DO (Leach) and NMSS EO (Piccone). | | | | * * * UPDATE 2037 EDT ON 8/29/99 FROM KEVIN BEASLEY TO S. SANDIN * * * | | | | The following information was provided as an update to this report: | | | | "Two adjacent sprinkler heads on C-337 System D-15 were identified to have | | corrosion and the PSS declared the system inoperable at 0925 [CDT] on | | 8/29/99. Also two adjacent heads on C-337 System D-10 were identified to | | have corrosion and the PSS declared the system inoperable at 1450. LCO | | required fire patrols for both of the affected areas were initiated in the | | time frame required by TSR. The PSS determined that an update to this | | report was required." | | | | Paducah personnel informed the NRC resident inspector. The NRC operations | | officer notified the R3DO (Leach) and NMSS EO (Piccone). | | | | * * * UPDATE AT 0930 EDT ON 9/1/99 BY ERIC WALKER TO FANGIE JONES * * * | | | | Add two adjacent sprinkler heads on C-337 D-14. Paducah personnel informed | | the NRC Resident Inspector. The NRC operations officer notified the R3DO | | (David Hills) and NMSS (Robert Pierson). | | | | * * * UPDATE AT 1133 EDT ON 9/8/99 BY TOM WHITE TO FANGIE JONES * * * | | | | Add two adjacent sprinkler heads on C-331 System 26, system declared | | inoperable at 2155 CDT on 9/7/99. An LCO required fire patrol for the | | affected area was initiated in the time frame required by the TSR. Paducah | | personnel informed the NRC Resident Inspector. The NRC operations officer | | notified the R3DO (Monte Phillips) and NMSS (Josie Piccone). | | | | * * * UPDATE AT 0948 ON 9/30/99 BY ERIC WALKER TO DOUG WEAVER * * * | | | | Add two adjacent sprinkler heads on C-333 System B-15 were identified to | | have corrosion and the PSS declared the system inoperable at 0815 on | | 9/30/99. An LCO required fire patrol for the affected area was initiated in | | the time frame required by the TSR. The PSS determined that an update to | | this report was required. | | Paducah personnel informed the NRC resident inspector. The NRC operations | | officer notified the R3DO (Vegel) and NMSS (Cool). | | | | | | *** UPDATE ON 10/13/99 @ 1600 BY WALKER TO GOULD *** | | | | Two adjacent sprinkler heads on C-333 System A-11 were Identified to have | | corrosion and the PSS declared the system inoperable at 1307 on 10-13-99. An | | LCO required fire patrol for the affected area was initiated in the time | | frame required by the TSR, The PSS determined that an update to this report | | was required. Paducah personnel informed the NRC resident inspector. The | | NRC operations officer notified the R3DO (Madera) and NMSS (Moore). | | | | * * * UPDATE 1520 10/19/1999 FROM UNDERWOOD TAKEN BY STRANSKY * * * | | | | Six sprinkler heads on C-337 System D-16 were identified to have corrosion | | and the PSS declared the system inoperable at 1052 CDT on 10/19/99. An LCO | | required fire patrol for the affected area was initiated in the time frame | | required by the TSR. The PSS determined that an update to this report was | | required. The NRC resident inspector has been informed of this update. | | Notified R3DO (Jorgensen). | | | | * * * UPDATE 2140 10/19/1999 FROM WALKER TAKEN BY STRANSKY * * * | | | | Seven sprinkler heads on C-337 System A-7 were identified to have corrosion, | | and another four had been painted over. In addition, three adjacent | | sprinkler heads pm C-337 System A-8 were identified to have corrosion. The | | PSS declared the systems inoperable at 1900 CDT on 10/19/99. LCO required | | fire patrols for the affected areas were initiated in the time frame | | required by the TSR. The PSS determined that an update to this report was | | required. The NRC resident inspector has been informed of this update. | | Notified R3DO (Wright). | | | | * * * UPDATE AT 1713 ON 10/21/99 FROM CAGE TAKEN BY JOLLIFFE * * * | | | | Four sprinkler heads on C-337 System A-5, twelve sprinkler heads on C-337 | | System A-8, three sprinkler heads on C-337 System A-9, and six sprinkler | | heads on C-337 System B-8 were identified to have corrosion. On 10/21/99, | | the PSS declared System A-5 and A-9 inoperable at 1028 CDT, System A-8 | | inoperable at 1227 CDT and System B-8 inoperable at 1406 CDT. An LCO | | required fire patrol for the affected areas was initiated in the time frame | | required by the TSR.. The PSS determined that an update to this report was | | required. The NRC Resident Inspector has been informed of this update. The | | NRC Operations Officer notified R3DO Bruce Jorgensen. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36079 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 08/27/1999| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 06:48[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/27/1999| +------------------------------------------------+EVENT TIME: 06:00[EDT]| | NRC NOTIFIED BY: DAVE WALSH |LAST UPDATE DATE: 10/21/1999| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |KATHLEEN MODES R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY SERVICE WATER SYSTEM DEGRADATION (ONLY ONE OF FOUR PUMPS | | OPERABLE) | | | | The following text is a portion of a facsimile received from the licensee: | | | | "On 08/26/99, Susquehanna Unit 1 and Unit 2 were operating at 100% power | | with the 'B' loop of emergency service water [(ESW)] out of service for | | scheduled maintenance. During testing on the ESW system, with all ESW pumps | | in service, it was identified that the 'C' and 'D' ESW pumps' discharge | | check valves were closed. The ESW flow surveillance was performed, and the | | 'C' and 'D' ESW pumps failed to achieve the required flow and were declared | | inoperable. Concurrently, the 'B' loop of ESW was returned to service. | | During the time the 'B' ESW loop was inoperable, the 'A' ESW pump was the | | only one operable ESW pump. This constitutes a serious degradation of the | | plant in that it is a condition which is outside of design basis and, | | therefore, reportable under 10 CFR 50.72(b)(1)(ii) requiring a 1-hour ENS | | notification." | | | | The licensee notified the NRC resident inspector. | | | | * * * UPDATE 1453EDT ON 9/3/99 FROM GRANT FERNSLER TO S. SANDIN * * * | | | | "This Notification is a retraction of a previous ENS Notification made | | 8/27/99 (Event # 36079)." | | | | "Subsequent evaluation by Engineering has concluded that the plant had at | | least two Emergency Service | | Water pumps capable of performing their specified safety function at all | | times. As such, the plant was not | | in a condition outside of its design basis and the report previously made | | pursuant to 10CFR50.72(b)(1)(ii) | | is hereby retracted." | | | | The licensee informed the NRC Resident Inspector. Notified R1DO(Rogge). | | | | * * *UPDATE 0316EDT ON 09/23/99 FROM MIKE PEAL TAKEN BY MACKINNON* * * | | | | The licensee is Retracting the Retraction they called in on 09/03/99 at | | 1453EDT. | | | | "On 09/22/99 at 2230, an Engineering evaluation concluded that the | | operability determination associated with the above stated event was not | | adequate, specifically relating to the potential for pump interaction to | | create low flow conditions. " | | | | "The Engineering evaluation was being performed in response to an anomaly | | identified on 09/20/99 during the run of 'D' Diesel Generator. During the | | preparation of the operability statement for the 09/20/99 anomaly, | | engineering personnel realized that incorrect assumptions were used in the | | previous operability statement. The 'C' and 'D' ESW pumps were declared | | inoperable at 2230 on 09/22/99. Evaluation continues to determine if other | | combinations of equipment out of service times result in additional | | reportable conditions." R1DO (Bob Summers) notified. | | | | The NRC Resident Inspector will be notified of the Retraction to the | | Retraction of this event by the licensee. | | | | * * * UPDATE AT 1325 ON 10/21/99 BY MIKE PEAL TO JOLLIFFE * * * | | | | Based on additional evaluations by Licensee Engineering, Operations and | | Licensing spanning the time frame of 06/03/99 to 09/28/99, the licensee | | concluded that the plant had at least one Emergency Service Water Pump per | | loop capable of performing its specified safety function at all times. As | | such, the plant was not in a condition outside of its design basis, was not | | in an unanalyzed condition, and there was no loss of safety function. The | | report previously made pursuant to 10CFR50.72(b)(1)(ii) on 09/23/99 is | | hereby retracted. | | | | The licensee plans to notify the NRC Resident Inspector. | | | | The NRC Operations Officer notified the R1DO Bill Cook. | +------------------------------------------------------------------------------+ !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36255 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SOUTH TEXAS REGION: 4 |NOTIFICATION DATE: 10/02/1999| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 21:03[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 10/02/1999| +------------------------------------------------+EVENT TIME: 19:05[CDT]| | NRC NOTIFIED BY: FRAWLEY |LAST UPDATE DATE: 10/21/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |JEFF SHACKELFORD R4 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 94 Power Operation |94 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNACCOUNTED FOR ACCESS KEY. COMPENSATORY MEASURES WERE PUT INTO PLACE. | | | | SEE HOO LOG FOR DETAILS. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | * * * UPDATE AT 1658 ON 10/21/99 BY KATHLEEN WORK TO JOLLIFFE * * * | | | | THE LICENSEE DESIRES TO RETRACT THIS EVENT AS A REPORTABLE EVENT AND WILL | | LOG THIS EVENT IN THEIR SAFEGUARDS EVENT LOG SINCE SECURITY IMPLEMENTING | | COMPENSATORY ACTIONS WERE IMPLEMENTED WITHIN 15 MINUTES FROM THE TIME THE | | LICENSEE DISCOVERED THAT THE KEY WAS MISSING. | | | | SEE THE HOO LOG FOR DETAILS. | | | | THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. | | | | THE NRC OPERATIONS OFFICER NOTIFIED THE R4DO LINDA SMITH. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36325 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 10/21/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 08:37[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 10/20/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 10:30[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 10/21/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE JORGENSEN R3 | | DOCKET: 0707002 |BRIAN SMITH EO NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: LARSON | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR 91-01 BULLETIN RESPONSE | | | | ON 10/20/99 AT 1030 HOURS, A NUCLEAR CRITICALITY SAFETY ANALYSIS (NCSA) | | NONCOMPLIANCE WAS IDENTIFIED IN THE X-330 PROCESS BUILDING. THIS | | NONCOMPLIANCE WAS DISCOVERED WHILE REVIEWING OBSERVATIONS FOUND DURING A | | WALKDOWN OF IMPLEMENTED NCSAs. | | | | AT COLUMN C-53 ON THE CELL FLOOR OF X-330, A DRIP PAN CONNECTED TO A PAIR OF | | LUBE OIL STRAINERS DID NOT MEET THE REQUIREMENTS OF NCSA-PLANT054 FOR LUBE | | OIL SYSTEMS. NCSA-PLANT054 REQUIRES ALL LUBE OIL LEAK COLLECTION CONTAINERS | | IN AREAS WHERE SIGNIFICANT UF6 RELEASES ARE CONSIDERED CREDIBLE, MEET | | CERTAIN SIZE RESTRICTIONS. IN X-330, THE MAXIMUM ALLOWED DEPTH OF A LUBE OIL | | DRIP PAN ON THE CELL FLOOR IS 3.6 INCHES. THE DRIP PAN FOUND WAS 5.76 INCHES | | DEEP. THIS VIOLATES THE CONTAINER SIZE REQUIREMENT OF THE NCSA. THE DRIP PAN | | CONTAINED APPROXIMATELY 25 QUARTS OF OIL AT TIME OF DISCOVERY. THERE WAS NO | | EVIDENCE OF ANY UF6 RELEASES IN THE AREA. | | | | THE CONTAINER SIZE LIMIT WAS EXCEEDED RESULTING IN THE LOSS OF GEOMETRY. THE | | OTHER CONTROL OF THE DOUBLE CONTINGENCY PRINCIPLE (CONCENTRATION) WAS | | MAINTAINED THROUGHOUT THIS EVENT. | | | | DOUBLE CONTINGENCY WAS REESTABLISHED BY OPENING AND TAGGING (DO NOT CLOSE) | | THE DRAIN VALVE IN THE BOTTOM OF THE DRIP PAN. THIS PREVENTS THE | | ACCUMULATION OF LUBE OIL TO A DEPTH GREATER THAN 3.6 INCHES. A WORK PACKAGE | | WAS DEVELOPED TO REMOVE THE DRIP PAN AND REPLACE IT WITH ONE THAT IS IN | | COMPLIANCE WITH NCSA-PLANT054. AT 1400 HOURS | | ON 10/20/99, THE NONCOMPLIANT DRIP PAN WAS REMOVED AND REPLACED WITH A PAN | | HAVING A DEPTH OF UNDER THREE INCHES, REESTABLISHING NCSA-PLANT054 | | COMPLIANCE. | | | | THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | | | THE NRC RESIDENT INSPECTOR AND THE DOE REPRESENTATIVE WERE NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 36326 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 10/21/1999| | UNIT: [1] [2] [] STATE: CA |NOTIFICATION TIME: 15:04[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 10/21/1999| +------------------------------------------------+EVENT TIME: 10:22[PDT]| | NRC NOTIFIED BY: DICK LUCKETT |LAST UPDATE DATE: 10/21/1999| | HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |LINDA SMITH R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - OFFSITE AGENCIES NOTIFIED OF A SPILL OF 3 OUNCES OF HYDRAULIC FLUID INTO | | PACIFIC OCEAN - | | | | THE LICENSEE NOTIFIED THE NATIONAL RESPONSE CENTER (EPA CASE #503190), THE | | CALIFORNIA OFFICE OF EMERGENCY SERVICES, AND THE NRC RESIDENT INSPECTOR OF A | | SPILL OF APPROXIMATELY THREE OUNCES OF BIODEGRADABLE HYDRAULIC FLUID FROM A | | KELP HARVESTER INTO THE PACIFIC OCEAN. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36327 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: ALLIED-SIGNAL INC. |NOTIFICATION DATE: 10/21/1999| | RXTYPE: URANIUM HEXAFLUORIDE PRODUCTION |NOTIFICATION TIME: 17:31[EDT]| | COMMENTS: UF6 CONVERSION (DRY PROCESS) |EVENT DATE: 10/21/1999| | |EVENT TIME: 16:00[CDT]| | |LAST UPDATE DATE: 10/21/1999| | CITY: METROPOLIS REGION: 3 +-----------------------------+ | COUNTY: MASSAC STATE: IL |PERSON ORGANIZATION | |LICENSE#: SUB-526 AGREEMENT: Y |BRUCE JORGENSEN R3 | | DOCKET: 04003392 |CHARLEY HAUGHNEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: HUGH ROBERTS | | | HQ OPS OFFICER: DICK JOLLIFFE | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |KBBF 70.50(b)(2)(ii) EQUIP DISABLED/FAILS | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | - PLANT FIRE WATER DELUGE SYSTEM LINE RUPTURED INSIDE THE PLANT - | | | | A SIX INCH RECTIFIER 'A' & 'B' PLANT FIRE WATER DELUGE SYSTEM LINE RUPTURED | | INSIDE THE PLANT. THE LICENSEE ISOLATED THE RUPTURE AND PLANS TO POST A | | FIRE WATCH AND REPAIR/REPLACE THE RUPTURED SECTION OF LINE. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 36328 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 10/22/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 03:01[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 10/21/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 10/22/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE JORGENSEN R3 | | DOCKET: 0707002 |CHARLEY HAUGHNEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SPAETH | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24 HOUR 91-01 BULLETIN RESPONSE | | | | On 10/21/ 1999 at 1500 hrs the Plant Shift Superintendent(PSS) was notified | | that a Nuclear Criticality Safety Approval (NCSA) requirement was not being | | performed in the X-710 ES&H Analytical Labs. NCS Engineering, while | | performing an NCS Self Assessment, noticed an operation where samples were | | brought to a staging area "INSIDE" a room when they were logged in and | | verified. (NCSA-0710_025.AOO) | | | | Requirement #1 of NCSA-071_25.AOO states in part; Samples in any room | | enriched to 1% or greater U-235, will be limited to one group of 30g U-235 | | per room. This will be ensured by maintaining a room inventory log of U-235 | | mass in labeled containers. Each log entry will consist of the U-235 mass | | value plus analytical uncertainty and will be: | | | | a. made by a knowledgeable person "PRIOR" to bringing the samples into the | | room, and | | b. verified by a second knowledgeable person "PRIOR" to bringing the samples | | into the room. | | | | At the direction of the Plant Shift Superintendent the requirements for an | | NCS anomalous condition were initiated and the area baundaried off. | | | | The safety significance of the event is very low. The U-235 mass in material | | is being maintained less than 30 grams as required. This is more than a | | factor of 10 less than the always safe mass of 350 grams U-235. The samples | | were brought to a staging area inside the room where they were logged in and | | verified. After logging and verifying the samples were moved to the | | operational area of the room, where they could interact with other materials | | in the room. | | | | Samples in any room enriched to 1% or greater U-235, with a concentration | | greater or equal to 500 ppm U-235, shall be limited to one group of 30 g | | U-235 per room. This shall be ensured by maintaining a room inventory log of | | U-235 mass in labeled containers. Each log entry shall consist of the U-235 | | mass value plus analytical uncertainty and shall be: | | | | Mass is the only parameter controlled | | | | The actual amount of material In the room is less than 30 grams U-235, at an | | enrichment of less than or equal to 100%. This value is obtained from sample | | data that was logged after the material was brought Into the room. This is | | approximately 4% of the worst case critical mass. | | | | Verbatim compliance with both mass controls was lost because the material | | was supposed to be checked and verified prior to bringing the material into | | the room. The samples were brought to a staging area inside the room where | | they were logged in and verified. After logging and verifying the samples | | were moved to the operational area of the room, where they could interact | | with other materials in the room. | | | | THERE WAS NO LOSS OF HAZARDOUS/RADIOACTIVE MATERIAL OR | | RADIOACTIVE/RADIOLOGICAL CONTAMINATION EXPOSURE AS A RESULT OF THIS EVENT. | | | | The Resident Inspector was notified and the DOE Representative will be | | notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021