Event Notification Report for May 26, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/25/1999 - 05/26/1999 ** EVENT NUMBERS ** 35751 35763 35764 35765 35766 35767 35768 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35751 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 05/21/1999| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 13:53[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 05/21/1999| +------------------------------------------------+EVENT TIME: 10:16[EDT]| | NRC NOTIFIED BY: MARK ELLINGTON |LAST UPDATE DATE: 05/25/1999| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ANN BOLAND R2 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INADVERTENT START OF THE 'B' CONTAINMENT SPRAY PUMP DUE TO AN INVALID START | | SIGNAL | | | | While performing the test of the Sequencer Block Circuit and Containment Fan | | Cooler, Train 'B' (#OST- 1095) with the plant at 100% power, a maintenance | | technician placed multimeter leads on the wrong terminal points. These | | terminal points were adjacent to the desired points. This caused an | | inadvertent start of the 'B' Containment Spray Pump. This invalid actuation | | was the result of an invalid signal generated by the maintenance technician. | | Investigation indicates that no other components actuated. | | | | The pump was aligned in standby and no flow was admitted to containment. | | The pump operated for approximately two minutes with adequate recirculation | | flow before it was secured. No equipment damage occurred and the 'B' | | Containment Spray system is currently operable. The licensee has | | conservatively determined that the pump start constitutes an ESF actuation. | | | | The NRC Resident Inspector was notified of this event by the licensee. | | | | * * * UPDATE AT 1817 ON 5/25/99 BY ELLINGTON, TAKEN BY WEAVER * * * | | | | On May 21, 1999, Harris Nuclear Plant performed a four hour non-emergency | | notification for an ESF actuation on the inadvertent starting of the B | | Containment Spray Pump. Harris Nuclear Plant has subsequently determined | | that no other components actuated nor would have actuated as a result of | | this event. The B Containment Spray Pump cannot by itself mitigate the | | consequences of an accident. In order for the Containment Spray System to | | mitigate the consequences of an accident, a downstream header isolation | | valve would have been required to open. This header isolation valve remained | | shut during this event. Harris Nuclear Plant has determined that this event | | was a single component actuation with no other components actuated and this | | single Component actuation could not have alone mitigated the consequences | | of an accident. Therefore, Harris Nuclear Plant retracts the May 21, 1999 | | four hour non-emergency notification per guidance provided in NRC | | NUREG-1022, Revision 1 page 53. | | | | The licensee will inform the NRC resident inspector. The HOO notified the | | R2DO (Decker). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35763 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MILLSTONE REGION: 1 |NOTIFICATION DATE: 05/25/1999| | UNIT: [] [2] [] STATE: CT |NOTIFICATION TIME: 15:58[EDT]| | RXTYPE: [1] GE-3,[2] CE,[3] W-4-LP |EVENT DATE: 05/25/1999| +------------------------------------------------+EVENT TIME: 15:28[EDT]| | NRC NOTIFIED BY: MICHAEL BAIN |LAST UPDATE DATE: 05/25/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP BECAUSE OF A SECONDARY SIDE STEAM LEAK | | | | The reactor was manually tripped from 100% power because of a steam leak in | | the 1A feedwater heater. All control rods fully inserted. Both motor | | driven Auxiliary Feedwater pumps were started and are maintaining water | | level in the steam generators. Decay heat is being removed by use of the | | steam generator atmospheric reliefs. | | The MSIVs are shut. The plant is stable in hot standby. | | | | The steam leak was discovered when oscillations in the feedwater heater | | water level resulted in a main control board annunicator. Personnel sent to | | investigate the feedwater heater reported a steam leak in the pipe leading | | up to the flange to which the relief valve is connected. Operators then | | manually tripped the reactor. | | | | Access to the turbine building is restricted while the feedwater heater is | | steaming down. A 120 V instrument AC panel switched to an alternate power | | supply during the plant transient. This had no effect on the plant's | | response. | | | | The licensee notified the NRC resident inspector and will notify state and | | local officials. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35764 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: THREE MILE ISLAND REGION: 1 |NOTIFICATION DATE: 05/25/1999| | UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 17:03[EDT]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP |EVENT DATE: 05/25/1999| +------------------------------------------------+EVENT TIME: 16:21[EDT]| | NRC NOTIFIED BY: JOHN SCHORK |LAST UPDATE DATE: 05/25/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PRESSURIZER SUPPORT BOLTS WOULD EXCEED ALLOWABLE STRESS DURING AN | | EARTHQUAKE | | | | At 1621 hours on May 25, 1999, utilizing preliminary calculations (not yet | | design verified), GPU Nuclear determined that a condition outside the design | | basis of the plant exists at TMI-1 and that an immediate report to the NRC | | in accordance with 10 CFR 50.72(B)(i)(ii)(B) is required. | | | | A review of the design of the bolts that insert into the Pressurizer Support | | Lugs found that in the event of the Safe Shutdown Earthquake (the Maximum | | Hypothetical Earthquake (MHE)) the bolts would be exposed to loads in excess | | of allowable stress as analyzed in the TMI-1 FSAR | | | | The bolts have been determined to be operable utilizing building and | | equipment damping factors (7% / 7%) in accordance with NRC Regulatory Guide | | 1.61. However, the TMI-1 FSAR utilizes more conservative damping factors (2% | | building / 2.5% equipment). When bolt load calculations are performed | | utilizing the FSAR factors, the MHE shear stress exceeds the allowable | | stress by approximately 25% and the MHE seismic stress slightly exceeds the | | allowable stress by approximately 1.5%. However, when the calculations are | | performed using the NRC Regulatory Guide 1.61 damping factors of 7% building | | / 7% equipment, the MHE shear and MHE seismic stresses are well within the | | allowable stress. | | | | GPU Nuclear intends to finalize the calculations and to resolve the | | non-conformance with the design basis as stated in the FSAR by either: | | | | Restoring the bolts to within the plant design basis via, the plant | | modification process or, | | | | Revising the plant design basis via a license amendment. | | | | This condition has been documented in the GPU Nuclear Corrective Action | | Program (CAP T1999-0264). | | | | The licensee will inform the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35765 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 05/25/1999| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 17:27[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 05/25/1999| +------------------------------------------------+EVENT TIME: 16:45[EDT]| | NRC NOTIFIED BY: RICK LANGE |LAST UPDATE DATE: 05/25/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | | |NLCO TECH SPEC LCO A/S | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE CORE SPRAY (HPCS) INOPERABLE | | | | "HPCS is inoperable but available. During an independent review of the In | | Service Inspection (ISI) program plan it was found that 52 welds in the HPCS | | system were improperly exempted from ISI requirements. These welds are | | located between the Condensate Storage Tank (CST) and the HPCS pump suction | | valve (MOV101). In addition, the weld inspections are required by ASME | | section XI. Preparations are being made to perform the required ISI weld | | exams." | | | | The HPCS LCO is 14 days. All other ECCS equipment is operable. | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35766 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/25/1999| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 21:29[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/25/1999| +------------------------------------------------+EVENT TIME: 19:24[EDT]| | NRC NOTIFIED BY: MARTIN MANTENFEL |LAST UPDATE DATE: 05/25/1999| | HQ OPS OFFICER: DOUG WEAVER +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD CONTE R1 | |10 CFR SECTION: | | |ADAS 50.72(b)(2)(i) DEG/UNANALYZED COND | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RCIC STEAM EXHAUST CHECK VALVES FAIL LEAK TEST | | | | TWO IN SERIES REACTOR CORE ISOLATION COOLING (RCIC) STEAM EXHAUST CHECK | | VALVES FAILED THEIR LEAK TESTS. THE LEAKAGE WAS IN EXCESS OF 10.1 GALLONS | | PER MINUTE. NO PRESSURE COULD BE ESTABLISHED IN THE LINE DURING THE TEST. | | THE PLANT IS SHUTDOWN IN REFUELING MODE SO RCIC IS NOT REQUIRED TO BE | | OPERABLE. CORRECTIVE ACTION WILL BE TAKEN BEFORE STARTUP. | | | | THE LICENSEE HAS NOTIFIED THE NRC RESIDENT INSPECTOR. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35767 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: WASHINGTON DEPARTMENT OF HEALTH |NOTIFICATION DATE: 05/25/1999| |LICENSEE: UNIVERSITY OF WASHINGTON |NOTIFICATION TIME: 23:52[EDT]| | CITY: SEATTLE REGION: 4 |EVENT DATE: 11/21/1998| | COUNTY: STATE: WA |EVENT TIME: 12:00[PDT]| |LICENSE#: WN-C001-1 AGREEMENT: Y |LAST UPDATE DATE: 05/25/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |THOMAS ANDREWS R4 | | | NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: TERRY FRAZEE | | | HQ OPS OFFICER: DOUG WEAVER | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | This is notification of an event in Washington state as reported to the | | WA Department of Health, Division of Radiation Protection. | | | | STATUS: new/closed | | | | Licensee: UNIVERSITY OF WASHINGTON | | City and state: SEATTLE, WA | | License number: WN-C001-1 | | Type of license: ACADEMIC BROAD SCOPE | | 9 | | Date of Event: Unknown | | Location of Event: Seattle, WA | | ABSTRACT: An "ownerless" surplus gas chromatograph (and detector cell) | | was being stored in a hallway at the University. An inventory check in | | late December 1998 noted the unit was no longer in the hallway and was | | presumed to have been put into better storage. By late January 1999, | | further checking had revealed that the unit probably had been taken to | | the UW Surplus Property Department. Records indicated the unit probably | | had been sold at auction on November 21, 1998 (there is some uncertainty | | because some items having no apparent value were discarded prior to the | | auction). The University RSO contacted the complete list of buyers in an | | attempt to recover the unit, however none of the buyers remembered | | acquiring a gas chromatograph at the auction. Some buyers also noted | | discarding items which had no apparent value immediately after the | | auction. The RSO has determined that the unit was most likely discarded | | in the trash in November either by UW Surplus Property Department or by | | one of the buyers. A contributing cause to this loss was failure of the | | Surplus Property Staff to notify the UW Radiation Safety Office of the | | auction. UW Radiation Safety routinely conducts "walk-through" | | inspections prior to auctions and as worked with Surplus Property Staff | | to help them identify hazardous equipment. There was no explanation why | | the Radiation Safety Office had been removed from the auction | | announcement database. This was corrected. There is little likelihood | | of human exposure to the radioactive source if it was sent to the | | landfill for disposal with the other trash. | | | | What is the notification or reporting criteria involved? WAC | | 246-221-240(1)(b) Reporting the loss of radioactive material in a | | quantity requiring notification within 30 days of occurrence. | | | | Activity and Isotope(s) involved: 15 millicuries of Ni-63 as of November | | 1, 1997 | | | | Lost, Stolen or Damaged? (Mfg., Model, serial number) Perkins-Elmer gas | | chromatograph source model B3C0119, serial number 3512. | | Leak test? Source was last leak tested on September 19, 1998. No | | indication of leakage. | | Disposition/recovery: Source is believed to have been discarded into the | | trash sent to a landfill. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35768 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/26/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 04:29[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/25/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 21:05[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/26/1999| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |TONY VEGEL R3 | | DOCKET: 0707002 | NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: RON CRABTREE | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 24-HOUR NRC BULLETIN 91-01 REPORT INVOLVING THE LOSS OF ONE OF THE TWO | | DOUBLE CONTINGENCY CONTROLS | | | | "On 5/25/99 at 2105 hours, while processing waste water solution through | | X-705 microfiltration filter press 'A', approximately 5 gallons of solution | | leaked from between the second and third filter plates, spilling onto the | | floor. At the time of this spill, Operations personnel were processing a | | 2072 liter 'batch' of waste water which contained 29.44 grams of U-235 at an | | enrichment of 1.4 wt % U-235. Plant Nuclear Criticality Safety Personnel | | determined the leak to be a loss of a single control (physical integrity of | | the system) such that only one of the double contingency controls (geometry) | | remained in place. | | | | "This event is reportable under NRC Bulletin 91-01, 24-hour criticality | | control. | | | | "There was no radioactive / radiological exposure as a result of this | | event. | | | | "SAFETY SIGNIFICANCE OF EVENTS: | | On May 25, 1999, approximately 5-gallons of concentrate leaked from filter | | press A in the microfiltration system. The leak occurred between the second | | and third filter press plates, most likely the result of a failed 0-ring. | | NCSA.0705_076 covers the use of inadvertent containers in X-705, given the | | concern of leaks/spills from the various solution bearing systems. | | NCSA.0705_076 considers the leak/spill of more than 4.8-liters from any | | system to be an unlikely event, given the design and physical integrity of | | the systems (i.e., the systems are designed and built to contain the | | solution). While this leak resulted in greater than 4.8-liters spilling from | | the system in question, the second contingency was not violated in that the | | solution did not accumulate in an unsafe geometry (it spilled to the floor | | and spread out into a safe slab geometry). | | | | "Based on sampling and batching calculations performed on the concentrate | | storage tank (i.e., T.103A) the total mass of material to be fed to the | | filter press is known prior to introducing concentrate into the filler | | press. NCSA-0705_015 limits the mass of U-235 to be processed (i.e., in a | | single batch) to a maximum of 350 grams. Per the filter press batch sheet | | for batch 103A-511, the batch being fed when this leak occurred contained | | 29.44 grams U-235. This amount of material is well below the safe mass of | | material, even at 100 wt% enrichment (ref. GAT-225). The actual enrichment | | of the material being processed was 1.4% U-235, per the filter press batch | | sheet for batch 103A-511. Therefore, while one of the contingencies was | | lost, the safety significance for this occurrence was low given the | | prerequisite for limiting the mass in the batch to 350 grams U-235. | | | | "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIO[S] OF HOW | | CRITICALITY COULD OCCUR): | | A significant amount of uranium-bearing solution would have to leak from a | | system and accumulate in an unsafe geometry in order for a criticality to | | occur. | | | | "CONTROLLED PARAMETERS (MASS, MODERATION, GEOMETRY, CONCENTRATION, ETC.): | | The parameters being controlled for this event were volume of a leak in a | | system in X-705. NCSA-0705_076 considers it unlikely that a leak of more | | than 4.8-liters would occur given the physical integrity of systems in | | X-705. In addition, the mass of U-235 in the batch being processed was | | limited to a maximum of 350 grams. | | | | "ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS | | LIMIT AND % WORST CASE OF CRITICAL MASS): | | Based on PR-PST-99-02948 and filter press batch sheet for batch 103A-511 | | the volume of solution which leaked was approximately 5-gallons. The maximum | | amount of U-235 in the concentrate was 29.44 grams and the maximum | | enrichment of material was 1.4 wt% U-235. It should be noted that the actual | | mass of U-235 which was in the leaked solution would be less than 29.44 | | grams, since the total amount of solution being processed was 2072 liters. | | | | "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION | | OF THE FAILURES OR DEFICIENCIES: | | NCSA-0705_075 considers it unlikely that more than 4.8-liters of solution | | would leak from a system given the physical integrity of the systems used in | | X-705. The leak in question resulted in approximately 5-gallons of solution | | leaking from the filter press. This amount of solution exceeded the | | considered limit for the unlikely event and resulted in the loss of double | | contingency for this leak. | | | | "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEM AND WHEN EACH WAS | | IMPLEMENTED:" | | | | Operations informed the NRC resident inspector and will inform the DOE site | | representative. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021